Blacksburg, VA, USA
N26VT
Pelt Mad Max II Special
The pilot and passenger intended to conduct a local flight in the amateur-built gyroplane, which was equipped with a Subaru EJ-22 automotive engine. The passenger placed two telephone calls prior to departing on the accident flight, and stated that the pilot was experiencing some type of mechanical difficulties with the gyroplane. According to the pilot, after a normal takeoff, the engine lost total power without any prior warning. The gyroplane was about 400 feet above ground level, and with no suitable terrain available for a forced landing, the gyroplane impacted a tree. It then fell about 40 feet to the ground and was engulfed in a post crash fire A Federal Aviation Administration (FAA) inspector examined the "severely burned" wreckage following the accident; however, given the condition of the wreckage, he was unable to determine a specific cause for the loss of engine power.
On October 6, 2007, at 1307 eastern daylight time, an amateur-built Mad Max II Special gyroplane, N26VT, was substantially damaged when it impacted trees and terrain during a forced landing near Blacksburg, Virginia. The certificated private pilot/builder was seriously injured, and the passenger was fatally injured. Visual meteorological conditions prevailed, and no flight plan was filed for the local flight, which originated at Virginia Tech Executive Airport (BCB), Blacksburg, Virginia. The personal flight was conducted under 14 Code of Federal Regulations Part 91. During a telephone interview, the pilot described some of the maintenance history of the gyroplane, and recounted the events of the accident flight. According to the pilot, he originally built the gyroplane in 2001, and at that time it was a single seat configuration. Between 2006 and 2007, he converted the gyroplane to a two seat configuration, and performed work on the engine, which included replacing "everything" with the exception of the carburetor and ignition coil. At the time of the conversion, the gyroplane had accumulated 175 total flight hours. Between the conclusion of the conversion and the accident flight, the pilot stated that he had completed the required test period, and flown the gyroplane for about 20 additional flight hours. About 10 of those 20 hours were flown with a person occupying the second seat. After takeoff on the accident flight, the pilot made a left turn about 400 feet above ground level, and in the airport traffic pattern. The engine was running normally for the first 1 to 2 minutes of the flight, when the engine "just flat out stopped." The pilot further described that the engine did not sputter prior to stopping, and that after the engine ceased producing power, the gyroplane began to sink. During the autorotative descent, the gyroplane performed as the pilot expected it to, and he attempted to diagnose the engine problem by checking the circuit breakers, all of which were nominal. Due to the trees and other obstructions below, the pilot was unable to locate a suitable forced landing site. The main rotor subsequently contacted a tree, separating it from the gyroplane, which then fell about 40 feet to the ground. The pilot additionally stated that about one month prior to the accident, he had a problem with the engine not reaching full power. While troubleshooting the issue, the pilot replaced the spark plugs, to no avail, but the issue resolved when he replaced the spark plug wires. He had flown the gyroplane about 10 hours since that time. He did not mention any other maintenance activities that he had performed during the interview. During a telephone interview, the passenger's mother stated that she received a phone call from the passenger on the morning of the accident flight. The passenger stated that she and the pilot would be delayed for their scheduled fly-over. The passenger further described that the gyroplane was having a problem "lifting properly," and that the pilot was checking the spark plug wires. The passenger also called a friend to advise her of the delay, and stated that they were "having problems getting the [gyroplane] up to full power." A pilot was performing an instrument approach to BCB in an airplane around the time of the accident. According to the airplane pilot, he initially transmitted his position and intentions on the airport UNICOM frequency. The pilot heard a reply from the accident pilot, who stated that he was maneuvering in the area for photography. The accident pilot stated that he would watch for and stay clear of the airplane pilot. When the airplane pilot was about 2 miles from the runway, he heard the accident pilot call "engine out" over the radio. While on short final approach, the airplane pilot observed black smoke rising about 1/2-mile from the runway. Several witnesses observed the gyroplane during the final portion of the flight. They reported that the engine was "stalled," or had "cut-off." One witness stated that the engine was "smoking" and that it "backfired once and shut off." One witness stated it appeared that the pilot was attempting to land in a residential yard. Another witness watched the gyroplane "fly over tree line, stall, then fall to ground." They all responded to the scene in order to render assistance, and found the gyroplane engulfed in flames. The pilot held a private pilot certificate with a rating for rotorcraft-gyroplane. His most recent Federal Aviation Administration (FAA) third class medical certificate was issued on January 22, 2007. On that date the pilot reported 175 total hours of flight experience. An FAA inspector examined the wreckage on October 10, after it had been recovered to BCB. The inspector established flight control continuity, and described that the gyroplane was "severely" burned. Valvetrain continuity could not be established, as the timing belt of the Subaru EJ-122 automotive engine was burned, but the crankshaft and both overhead camshafts were able to rotate. Removal of the engine heads and examination of the engine interior revealed no signatures consistent with pre-ignition or detonation. All 4 Bosch part number FR9DPX spark plugs were removed, and appeared "new" with a "slight heat discoloration" of the ground electrode. The oil sump, cooler, and filter all contained oil, and examination of the oil filter revealed no evidence of any metallic particles. The 4-barrel carburetor was melted by fire, but both of the throttle arms and the accelerator pump arm were free to move. The carburetor mounting bolts remained attached, but were secured "loose[ly]." Measurement of the rotor system revealed that each blade was 13 feet long, forming a 26-foot rotor diameter. According to the FAA, the gyroplane was built by the pilot, and its experimental airworthiness certificate was issued on July 21, 2001. Examination of weight and balance information revealed that the basic empty weight of the gyroplane was 673 pounds. In May 2007, the pilot installed a second seat into the gyroplane. The updated basic empty weight of the gyroplane in the two-seat configuration was 708 pounds. The gyroplane had a fuel capacity of 14 gallons. Review of the gyroplane's maintenance records revealed that the most recent condition inspection was completed on June 2, 2007. The weather conditions reported at BCB, about 1 nautical mile southwest of the accident site, at 1300, included winds from 090 degrees at 7 knots, 10 statute miles visibility, scattered clouds at 3,800 feet, a broken ceiling at 5,000 feet, temperature 73 degrees Fahrenheit, dewpoint 64 degrees Fahrenheit, and an altimeter setting of 30.30 inches of mercury.
A loss of engine power for undetermined reasons. Contributing to the accident was a lack of suitable terrain for a forced landing.
Source: NTSB Aviation Accident Database
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