Norridgewock, ME, USA
N179TC
Christopher John P CHR-1
The pilot of the gyroplane stated that after takeoff he climbed to pattern altitude and, while on downwind and abeam the runway numbers, he heard a “pop and then experienced a terrible, violent vibration, seemingly catastrophic in nature. There was no power, but the engine was still running.” As he was conducting a forced landing in rough terrain, the wheel and then the main rotor dug into the ground, causing the ship to roll onto its side. The main rotor, mast, landing gear, and horizontal stabilizer sustained damage. Further examination by the pilot revealed that the engine crankshaft was broken near the No. 1 cylinder. The pistons of the non-certified engine had been replaced about 10 operational hours earlier.
On July 30, 2009, about 1800 eastern daylight time, an experimental, amateur-built CHR-1, N179TC, was substantially damaged during a forced landing at Central Maine Airport (OWK), Norridgewock, Maine. The gyroplane was registered to a private individual. The certificated commercial pilot was not injured. Day visual meteorological conditions prevailed at the time, and no flight plan was filed for the 14 Code of Federal Regulations Part 91 personal flight. The flight originated at OWK at 1745. The pilot stated that after takeoff, he climbed the gyroplane to pattern altitude, and while on downwind and abeam the runway numbers, he heard a “pop and then experienced a terrible, violent vibration, seemingly catastrophic in nature. There was no power, but the engine was still running.” He said that he was over a landfill, which was the closest site for an emergency landing. During the flare/touchdown, the right wheel caught on rough terrain damaging the mast, main rotor, right landing gear and the horizontal stabilizer. The gyroplane was powered by a 66-horsepower Rotax 583 engine, with about 100 hours of operation since new. An inspector from the Federal Aviation Administration (FAA) reported that the gyrocopter’s last condition inspection was accomplished on May 23, 2009. The owner/pilot stated to the inspector that the engine was about 10 hours out of overhaul, which included new pistons. On scene examination of the airframe found fuel in the fuel tank, and fuel filters, with no contamination noted. Examination of the intake manifold found the number 2 intake with black oily residue around the area and no residue around the number 1 intake. Further examination by the owner/pilot revealed that the engine crankshaft was broken near the number 1 cylinder.
A loss of engine power due to a broken crankshaft for undetermined reasons.
Source: NTSB Aviation Accident Database
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