Salt Lake City, UT, USA
N373C
STINSON 108-2
During cruise flight, the pilot experienced a complete loss of engine power and initiated a forced landing to an open field. During the landing roll, the airplane encountered a ditch, which resulted in substantial damage to the airplane's fuselage. A Federal Aviation Administration airworthiness inspector reported damage to the accessory section of the engine. A subsequent postaccident examination of the engine by a second inspector revealed that the crankshaft gear had failed, which resulted in significant damage to all the gears in the accessory section of the engine. Over 50 percent of the crankshaft gear could not be found, and the crankshaft gear appeared to have fractured and failed through both dowel pin slots. The engine was manufactured in 1947 and was the original engine installed by the factory at the time of the airframe's manufacture. The engine had accumulated 2,520 hours time in service and was overhauled 147 hours prior to the accident.
On August 3, 2009, about 1315 mountain daylight time, a Stinson 108-2, N373C, sustained substantial damage after making a forced landing due to a total loss of engine power about 2 miles east of the Salt Lake City International Airport (SLC), Salt Lake City, Utah. The commercial pilot was not injured, and the sole passenger sustained minor injuries. Visual meteorological conditions prevailed for the cross-country flight, which was operated in accordance with Title 14 Code of Federal Regulations (CFR) Part 91, and a flight plan was not filed. The flight departed the Rock Springs-Sweetwater County Airport (RKS), Rock Springs, Wyoming, about 1130, and was destined for the Bolinder Field-Tooele Valley Airport (TVY), Tooele, Utah. The pilot reported that while in cruise flight at 10,500 feet mean sea level (msl) "…the engine suffered a catastrophic failure." The pilot stated that he set up a glide for SLC, but seeing he was not going to make it he elected to land in an field east of the airport. The airplane sustained substantial damage to the fuselage in the area where both main landing gear were attached. A Federal Aviation Administration (FAA) airworthiness inspector, who responded to the accident site, reported damage to the accessory section of the Franklin 6A4-165 engine. A subsequent post-accident examination of the engine by a second inspector revealed that the crankshaft gear had failed, which resulted in the damage to the accessory section of the engine. The inspector further reported that all accessory gears exhibited mechanical damage. Over 50 percent of the crankshaft gear could not be found, and that the crankshaft gear appeared to have failed at both dowel pins slots. The engine was a Franklin 6A4-165B-3 that was manufactured in 1947 and was the original engine installed by the Stinson factory at the time of the airframe manufacture. The engine had accumulated 2,520 hours time in service and was overhauled 147 hours prior to the accident.
A total loss of engine power during cruise flight due to the failure of the crankshaft gear.
Source: NTSB Aviation Accident Database
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