Aviation Accident Summaries

Aviation Accident Summary WPR10LA051

Tucson, AZ, USA

Aircraft #1

N2165M

PIPER PA-32R-300

Analysis

While descending for landing, the engine lost partial power and the airplane could not maintain altitude. The pilot attempted to divert to a nearby airport; however, he was not able to arrest the airplane's descent and had to make a forced landing to a road. The pilot stated that about 20 feet above the ground, he believes the engine lost all power. The airplane landed hard, struck a road sign, departed the paved surface, and came to rest on the desert floor. A postaccident examination of the airplane and the fuel-injected engine revealed no mechanical anomalies that would have precluded normal operation.

Factual Information

On November 7, 2009, at 1700 mountain standard time, a Piper PA-32R-300, N2165M, experienced a partial loss of engine power in cruise flight and made an emergency landing on a highway about 32 miles northwest of the Tucson International Airport (TUS), Tucson, Arizona. The owner/pilot operated the airplane under the provisions of 14 Code of Federal Regulation Part 91, as a personal flight. The private pilot and one passenger were not injured. The airplane sustained structural damage to the fuselage after departing the highway and impacting a road sign and cacti prior to coming to rest upright. Visual meteorological conditions prevailed for the local area flight that departed Phoenix-Mesa Gateway Airport (IWA), Phoenix, Arizona, at 1616. No flight plan had been filed. According to the pilot's written statement, he had been cleared direct to TUS via global positioning system (GPS) at 6,500 feet mean sea level (msl). About 35 miles northwest of TUS, he started the descent to 4,500 feet msl. As the airplane passed through 5,000 feet, he configured the manifold pressure and rpm (24/2,400) per the airplane's pilot operating handbook (POH) for 4,000 feet at 75 percent power. Shortly thereafter, he felt the airplane 'lurch,' as if the engine had lost rpm's. He increased the engine power, the fuel mixture, and moved the propeller to the FULL in position in an attempt to get more engine power. The pilot stated that the engine continued to run, and the propeller was still spinning, it just was not enough power to hold altitude; he noted a 500-foot-per-minute descent that he was not able to arrest. The pilot radioed TUS to report a partial engine failure and his current position. TUS tower personnel gave him vectors to a closer airport; however, as he made the turn toward the airport, the airplane lost altitude too quickly and he knew that the airplane would not make the airport. The pilot stated that there was a road below the airplane and he attempted to land on the road. He believes that about 20 feet above the ground, the engine quit, and the airplane landed hard. Upon touchdown, he heard a 'thud' and ascertained that the airplane had departed the roadway and onto the adjacent desert floor. After the accident, the pilot reported that the airplane had struck a road sign. An engine inspection was performed by investigators from the National Transportation Safety Board (NTSB) and from Lycoming Engines. Under the supervision of the NTSB investigator, the cowling was removed. There were no obvious signs of a mechanical failure. All fuel lines were secure, and no fluid leaks were observed. The magnetos were secure and tight on their respective mounting pads. Manual rotation of the propeller produced thumb compression in all six cylinders. The servo plug remained in place and was secured by safety wire. No mechanical anomalies were noted that would have precluded normal operation.

Probable Cause and Findings

A loss of engine power for undetermined reasons.

 

Source: NTSB Aviation Accident Database

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