West Palm Beach, FL, USA
N884
AIR GULFSTREAM AIRLINES INC SX-300
The pilot stated that the airplane began to track to the right immediately after touchdown on runway 15. He applied left rudder and full power in an attempt to go around and the airplane lifted briefly, but then touched down off the right side of the runway. Upon contact with the unimproved surface, all three landing gear collapsed, resulting in substantial damage to the airplane. The nearest official weather reporting station, approximately 5 miles to the north of the accident site, reported that the winds were from 010 degrees at 6 knots. The pilot indicated that there was a mechanical malfunction with the brakes or landing gear that caused the airplane to track to the right upon touchdown. He also stated that he successfully performed a brake check prior to the flight, and that the airplane was tracking normally during the takeoff roll. Examination by an airframe and power plant mechanic revealed that the right main gear upper trunnion mount and the left main landing gear scissor were broken. All components of the brake system were in “very good, operational, condition” and there was no evidence of any preexisting anomalies with either the brakes or the landing gear.
The pilot stated that the airplane began to track to the right immediately after touchdown on runway 15. He applied left rudder and full power in an attempt to go around, and the airplane lifted briefly, but then touched down off the right side of the runway. Upon contact with the unimproved surface, all three landing gear collapsed resulting in substantial damage to the airplane. The nearest official weather reporting station approximately 5 miles to the north of the accident site showed the winds were from 010 degrees at 6 knots. The pilot indicated on the NTSB 6120.1, that there was a mechanical malfunction with the brakes or landing gear that caused the airplane to track to the right upon touchdown. He also stated that he successfully performed a brake check prior to the flight, and that the airplane was tracking normally during the takeoff roll. Examination by an airframe and power plant mechanic revealed that the right main gear upper trunnion mount and the left main landing gear scissor were broken. All components of the brake system were in “very good, operational, condition”, and there was no evidence of any pre-existing anomalies with either the brakes or the landing gear.
The loss of directional control while landing for undetermined reasons.
Source: NTSB Aviation Accident Database
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