Pacoima, CA, USA
N1231A
EUROCOPTER AS350B2
During a downwind departure from the airport, the engine began to lose power. The pilot initiated an immediate autorotation back toward the airport while adjusting the airspeed and flight controls to clear power lines along the airport boundary. After clearing the power lines, the helicopter settled hard on the runway centerline and then began to rock, slide, and yaw right. The pilot attempted to regain control of the helicopter, and it eventually came to a stop upright on its skids facing about 160 degrees right of the runway centerline. The aft portion of the tail boom had separated. Postaccident testing and examination of the engine revealed a degraded power turbine (PT) governor spool bearing. Examinations also revealed the presence of diamond particles, which are used in the manufacturing process for the ball bearings, in the governor spool bearing. It is likely that diamond particle contamination caused the governor spool bearing to fail, which rendered the PT governor incapable of modulating governor servo pressure to the fuel control unit. Although no physical evidence was found indicating that the electronic overspeed system activated, the pilot's statement about two increases in rpm and then a decrease in rpm indicates that the system likely activated. The loss of PT governing ability coupled with the activation of the electronic overspeed system likely resulted in fuel flow oscillations that decreased the fuel flow below the lean blowout limit of the engine and led to the loss of engine power.
HHISTORY OF FLIGHT On November 12, 2010, at 0748 Pacific standard time, a Eurocopter AS350B2, N1231A, experienced a loss of engine power shortly after departure from Whiteman Field, Pacoima, California. During the subsequent forced autorotation, the helicopter experienced a hard landing, and the tail boom separated. Tiny Bubbles Aviation, Inc., was operating the helicopter under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The commercial pilot and one passenger were not injured. The helicopter sustained substantial damage to the airframe. The local electronic news gathering (ENG) flight was departing at the time in visual meteorological conditions. No flight plan had been filed. The pilot stated that the helicopter lifted off from taxiway Alpha, and was parallel to runway 12. A climb was established, and all systems were in the normal operating range. The pilot proceeded on a right downwind departure, and planned to exit the airport area on a 45-degree angle. During the turn from the upwind to the downwind leg, he noticed a slight and momentary upward change in the sound of the engine revolutions per minute (rpm). The turn to downwind leg was normal, and remained so until he was abeam midfield and preparing for the left 45-degree departure. The pilot noted a second and much more pronounced rise in engine rpm, and thought that the engine might overspeed, so he began to lift the collective up to arrest the rpm rise, and prepare for a possible emergency governor operation. The pilot stated that in less than a second, the engine speed sound reversed from a high sound to a rapid rpm decrease. He immediately lowered the collective to the full-down position, adjusted the cyclic to establish a 60- to 65-knot attitude, and looked forward for a suitable landing area. The helicopter was in a stable, steady-state autorotation, but there was no area directly ahead for an emergency landing without causing an extreme hazard to homes and people on the ground. He turned the helicopter 90 degrees toward the airport, which was the only open area that he thought he could possibly reach. Upon rollout, he realized that at the current airspeed and rate of descent, the helicopter would not clear the 40-foot powerlines on the airport boundary. The pilot stated that he smoothly and firmly lowered the nose to an approximate 90-knot attitude. About 1 second later, he raised the collective lever, which increased the rotor pitch and extended the glide. After 3 to 4 seconds, it became apparent that the helicopter was going to clear the obstructions, and get to the airport property. At this time, he noted that the yellow GEN light was illuminated on the annunciator panel. The pilot determined that the airspeed and rate of descent were unacceptably high to perform a safe touchdown, and the helicopter was positioned 90 degrees to the runway centerline, and heading toward intersection Charlie, which had parked airplanes and the airport fuel pit just beyond it. Shortly before crossing the wires, he raised the nose back to the 60- to 65-knot attitude, and lowered the collective to the full down position. After crossing the wires, he aggressively rolled the helicopter into a left bank to align it with runway 30, and added a little collective pitch halfway through the turn. As he completed the turn, he again lowered the collective; the rate of descent had predictably climbed very high, and he raised the nose to trade airspeed to arrest the descent rate. The pilot added collective about 20 feet above ground level to further arrest the descent rate. He noted that neither of those inputs had the ideal effect, and the helicopter was settling far too rapidly. He then raised the collective further in an attempt to reduce the descent rate, lowered the nose, and firmly applied all remaining collective pitch just before the skids touched down. The helicopter's attitude was more nose high than he preferred, but with as much forward speed as it had, he felt that he had to hold that position. The helicopter settled hard on the runway centerline, but held a good position for a short time before it began to rock forward quite hard so the pilot countered with a smooth and steady aft cyclic input. As it settled back hard on the skids, he began to neutralize the cyclic. The helicopter was on the ground, aligned with the centerline, and sliding at 25 knots. As the fore and aft rocking stopped and the helicopter was solidly on the skids, it began a right yaw. The pilot applied full left anti-torque pedal to no effect as the helicopter continued to slide and yaw right. The pilot gently began rolling the cyclic to the right trying to time it to be at full deflection away from a possible left rollover as the helicopter began yawing through 90 degrees from the touchdown heading. The helicopter came to a stop, upright on the skids, and facing 160 degrees right of the centerline. The rotor blades were turning about 50 rpm, and the photographer on board voiced that they would wait until the rotor blades stopped before egressing. While the blades were stopping, the pilot turned off the electrical master switch and two fuel pumps, and moved the throttle lever to the idle cut-off position. After the blades stopped, they exited, and walked a safe distance away. The pilot noted that the aft 1/3 of the tail boom had separated, and was lying on the runway. He also noted white smoke emanating from the exhaust stack; it stopped smoking about 30 seconds later. The pilot estimated that the time from the power loss to the helicopter coming to rest was 18-23 seconds. AIRCRAFT The helicopter was a Eurocopter AS350B2, serial number 3682. The operator reported that the helicopter had a total airframe time of 3,456.5 hours at the time of the accident. It had a 100-hour inspection completed on October 5, 2010. The engine was a Honeywell LTS101-700D2 turboshaft, serial number LE-46130C. The original Turbomeca Aeriel 1D1 engine had been replaced in accordance with STC Number SR01647SE held by SOLOY, LLC. Total time recorded on the engine was 4,042 hours, and time since major overhaul was 546.5 hours. TESTS AND RESEARCH Follow Up Examinations Engine Investigators examined the engine at the Honeywell facilities in Phoenix, Arizona, from January 25-27, 2011. A detailed report is part of the public docket for this accident. January 25, 2011 During the initial visual evaluation, the engine was turned with a spline adapter tool in the starter pad to verify rotation of the Gas Producer (GP) section. The Power Turbine (PT) section rotated freely. At the conclusion of the evaluation, the engine was prepared for a run in a test cell. January 26, 2011 Prior to the first start attempt in a test cell, a borescope inspection of the bottom of the PT and compressor section identified no mechanical damage or contamination. Cranking the engine verified an increase in oil pressure. No metallic debris was noted on the gearbox chip detector. The first test run lasted approximately 6 minutes at idle; there was a residual fuel leak from plenum drain at shutdown. White smoke was noted to be emanating from the engine inlet for approximately 4-5 minutes following shutdown. The second test run lasted approximately 33 minutes. In accordance with the engine test instructions (TI), the engine was operated at ground idle and flight idle. A third test run lasted approximately 1 hour 31 minutes. The engine was operated in accordance with the TI, and verified the engine's ability to reach take-off power. During the PT governor check, the PT governor appeared to not govern the PT speed as the waterbrake was slowly unloaded. Power turbine speed (NPT) increased to 107 percent before the waterbrake was reapplied. The engine was then shut down, and rigged for an overspeed (o/s) protection check. January 27, 2011 The electronic overspeed system operation check was performed successfully using a Honeywell slave overspeed controller. Upon completion with the slave equipment, the accident helicopter's overspeed controller box was installed. The electronic overspeed system operation check was performed successfully using the accident helicopter's overspeed controller. An additional test was performed to verify the actual overspeed trip point. The overspeed protection system activated at 109.1 percent NPT, which was within limits, and three additional tests had the same results. A leak check of the pneumatic system was performed using a soapy water solution. Leaks were observed in the following locations: Px Bleed orifice threads Pc filter to T1 sensor at the Pc filter – note that this line was removed previously to facilitate removal of the engine from the helicopter. Pc filter t-fitting cap. The Power Turbine Governor (PTG) and Fuel Control Unit (FCU) line replaceable units (LRU's) were removed for further testing at the Honeywell facility in South Bend, Indiana. PTG and FCU Examinations Examination of the PTG and FCU were conducted on February 23, 2011, at the Honeywell Engines Systems and Services Facility in South Bend, Indiana. A complete report on the testing of the PTG and FCU is part of the public docket for this accident. PTG A functional test was not possible due to the inability to achieve the first test point; there was no PR-PG pressure signal. The ambient vent screen was removed in order to inspect the test bench coupling interface to the unit. The drive was correct and operative with no anomalies noted. Metal debris was observed on the throttle cam / cam lever assembly that was internal to the unit. The spool bearing cap showed excessive movement. Disassembly of the unit revealed that the spool bearing was not properly supporting the interfacing spool bearing cap. Spool bearing debris, which consisted of bearing retainer pieces and two loose balls, were in the drive body cavity. Examination of the inner race under magnification indicated shoulder wear noted in the direction of the governor (GOV) drive (toward GOV mount pad). FCU The FCU was Model DP-S1; part number 2549165-1; serial number 337045. During a visual inspection, the speed input drive shaft rotated freely. The throttle shaft rotated freely from minimum to maximum. A functional pneumatic air leak test on the Px-Py air circuit revealed zero leakage, which was normal. The fuel control unit was tested in accordance with Test Specification TS12991. Several parameters fell outside of test limits. Based on the results of the testing, the unit was not disassembled. Honeywell Materials Lab Testing Bearing pieces, inner and outer spool bearing race pieces, and debris were taken to the Honeywell materials laboratory for examination. A summary report of the findings is part of the public docket for this accident. Ball Inspection Scanning electron microscope (SEM) inspection indicated that there was material transfer and smearing. Dents and spalling were noted as well as embedded hard particles that were aluminum oxide and diamond. Inner Race Visual inspection revealed that the surfaces were rough in appearance. SEM inspection revealed substantial smearing, tearing, and roughness in the raceway. There were hard particles in the race that were diamond in appearance. The race damage was caused by hard particles, and hard particle damage was still occurring at the end of the failure. Outer Race SEM inspection revealed that hard particles with a diamond appearance were in the race. Materials Lab Summary Significant quantities of imbedded diamond particles were observed in the inner and outer races. A few diamond particles were imbedded on the surface of the sample ball. There was evidence of damage from the particles in the races; the race wear was significant. No external source of contamination could be identified. Diamond particles were used in the manufacturing process for the ball bearings. Honeywell Service Bulletin (SB) GT-73-351 Honeywell SB GT-73-351 (Revision 0, 7 July 2010) applied to this engine at the time of the accident. It required replacement of the spool bearing (part number 2523973N) with a new spool bearing (part number 2523973N) depending on time in service. It indicated a compliance time of 900 hours for bearing replacement. As a result of this accident, Honeywell issued SB GT-73-351 (Revision 2, 27 Jun 2011), which reduced the service life to 600 hours. Summary of Findings The testing and examination of the engine disclosed a degraded power turbine (PT) governor spool bearing, which rendered the PT governor incapable of modulating governor servo (Py) pressure to the fuel control. Postaccident examination of the engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation.
The contamination of a spool bearing in the power turbine governor during manufacture, which led to the bearing’s failure in flight, a subsequent loss of engine power during departure, and the resultant hard landing.
Source: NTSB Aviation Accident Database
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