Aviation Accident Summaries

Aviation Accident Summary WPR11LA074

Chino, CA, USA

Aircraft #1

N5800U

PIPER PA-28-140

Analysis

The certified flight instructor and student pilot had just performed a soft-field landing. During the subsequent rollout, they noted that the airplane was not taxiing as expected. As the airplane exited the runway, it dropped onto its left wing and spun to the left. Examination of the left main landing gear revealed that the upper torque-link attachment lugs had detached from the landing gear strut, causing separation of the wheel assembly and subsequent substantial damage to the left wing. Further metallurgical examination of the strut revealed evidence of preexisting fatigue cracks to the upper torque-link attachment lugs. The airplane manufacturer issued a Service Bulletin about 8 years prior to the accident requiring inspection of the lugs in the area of failure. No evidence was found suggesting that the Service Bulletin had been complied with.

Factual Information

On December 10, 2010, at 1558 Pacific standard time, a Piper PA-28-140, N5800U, sustained substantial damage to the left wing during taxi after landing at Chino Airport, Chino, California. DuBois Aviation operated the airplane under the provisions of Title 14 Code of Federal Regulations Part 91 as an instructional flight. The student pilot and certificated flight instructor (CFI) were not injured. The local instructional flight departed Chino about 1430. Visual meteorological conditions prevailed, and no flight plan had been filed. The CFI reported that after performing a soft-field landing, the airplane was not taxing as expected. As they exited the runway, the airplane dropped onto its left wing, and spun to the left. Examination of the left main landing gear strut (part number 65319-3) by the NTSB investigator-in-charge revealed that the upper torque-link attachment lugs had detached from the landing gear strut. Additionally, the wheel assembly had become separated from the strut, coming to rest against the aft underside surface of the wing. The wing sustained wrinkles to the upper and lower inboard skins, and three collapsed wing ribs were observed. Both the CFI and the student pilot reported performing an uneventful preflight inspection prior to the accident flight, noting no preexisting structural damage to the airplane. The landing gear strut and lugs were sent to the NTSB Materials Laboratory for further examination. Metallurgical examination revealed that both lug separation surfaces exhibited curving boundary features, and areas of discoloration indicative of preexisting cracks. New Piper Aircraft, Inc., issued Service Bulletin (SB) 1131 on August 18, 2003, requiring visual and dye penetrant inspections of "cast" main landing gear strut cylinders at the next regularly scheduled maintenance event (or within 100 hours), and at 100-hour intervals thereafter until the cylinder was replaced with a new forged part. The subject cylinder was of the "cast" type, with a serial number that was found to be within the SB's affected range. Examination of the airplane's maintenance logbooks revealed that this Service Bulletin had not been performed.

Probable Cause and Findings

Fatigue cracking of the upper torque-link attach lugs on the left main landing gear strut, which resulted in separation of the left main landing gear during taxi.

 

Source: NTSB Aviation Accident Database

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