Phoenix, AZ, USA
N7850P
CIRRUS DESIGN CORP. SR22
A review of radar data revealed that the single-engine Cirrus airplane entered the left downwind leg of the traffic pattern for runway 3 as a Gulfstream twin-engine corporate jet was 5 miles to the west for landing. The tower controller instructed the Cirrus pilot to extend his downwind leg to follow the Gulfstream and then instructed him to report when he had the Gulfstream in sight. The Cirrus pilot made his base turn towards the final approach course before reporting the Gulfstream in sight, which resulted in the Cirrus being in very close proximity to the Gulfstream. The Cirrus pilot had the discretion to turn from the extended downwind to the base leg prior to the controller advising him to do so; however, when he made this decision it then became his responsibility to maintain safe separation from the Gulfstream. After several traffic advisories from the controller to the accident pilot, the pilot finally reported the Gulfstream in sight, at which point the Gulfstream was about 0.11 nautical miles ahead of--and 200 to 300 feet higher than--the Cirrus on final to runway 3. The controller then radioed the Cirrus pilot to stand by for a possible go-around and the pilot replied that he was standing by. The controller instructed the Cirrus pilot to start a climb and go around. Three seconds later, an unidentified pilot radioed the controller that an airplane on final had just gone down; no further communications were received from the Cirrus pilot. About 7 seconds before the accident, the Cirrus was at an altitude of 1,400 feet above ground level. The Gulfstream had passed that location about 30 seconds earlier and 150 feet higher than the Cirrus. The upset and loss of control most likely occurred as a direct result of an encounter with the wake turbulence generated by the Gulfstream while the Cirrus was in trail and on final approach to the runway. An onboard recording device revealed that at 0954 the Cirrus experienced an upset, rolling rapidly from 35 degrees left-wing-down to over 77 degrees left-wing-down, before rapidly rolling to 25 degrees right-wing-down. At this time, the airplane's rate of descent was in excess of 3,000 feet per minute.
HISTORY OF FLIGHT On December 15, 2011, about 0954 mountain standard time, a Cirrus Design Corp. SR22, N7850P, experienced a loss of control and descended into a residential neighborhood about 0.75 nautical miles from the approach end of runway 3 at the Scottsdale Airport (SDL), Scottsdale, Arizona. The airplane was registered to Frank M. Smith & Associates, Inc., and it was operated by a company private pilot who was fatally injured. The passenger was seriously injured. The airplane was consumed by a post-impact fire. No one on the ground was injured during the impact sequence. The flight was performed under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed, and no flight plan was filed. The flight originated from Show Low Regional Airport (SOW), Show Low, Arizona, about 0913, with SDL as its planned destination. The surviving passenger reported in a post-accident interview with the NTSB investigator-in-charge (IIC), that the airplane was based at SOW, and that the pilot made routine flights to and from SDL. The passenger stated that prior to departure the pilot preflighted the airplane for about 30 minutes, and that nothing unusual occurred during the takeoff, climb, or during the en route phase of the flight, which was smooth. The passenger revealed that while approaching SDL, he recalled the controller asking the pilot if he saw the Gulfstream, and that the pilot asked him, "Do you see the Gulfstream?" The passenger reported that he initially did not see the Gulfstream, but when he looked outside his right-side window he saw it very close to the Cirrus. He added that at the time, the pilot was still looking left for the Gulfstream, and that he did not initially see it. The passenger stated that about the time when this occurred, the pilot was turning left toward the airport and that he was startled by the sudden presence of a dark shadow over the Cirrus as the Gulfstream passed overhead. The passenger further stated that the Gulfstream appeared to "fly on top of us." The passenger also opined that he did not recall seeing the Gulfstream again, and it was about this time that the controller asked the pilot again if he saw the Gulfstream. The passenger reported that the pilot replied to the controller that the Gulfstream was "in my back seat." He further reported that the pilot was startled by the close proximity between his airplane and the Gulfstream, and that he did not believe that the pilot had observed the Gulfstream prior to the close encounter of the two airplanes. The passenger recalled that it seemed like only seconds after the close encounter that the Cirrus started rapidly descending. The passenger did not recall anything further, including the impact sequence or how he exited the airplane after it had crashed. A review of radar data provided by Cirrus Aircraft Corporation, as well as communications between Federal Aviation Administration Air Traffic Control, N7850P (the accident airplane), and N534QS (the Gulfstream), revealed that the Gulfstream first contacted the SDL control tower at 0950:25, six nautical miles west of the airport. The controller instructed N534QS to enter a left base for runway 3. At 0950:44, N534QS turned to a heading of 142 degrees magnetic for the left base leg to runway 3. While on the base leg, N534QS slowed from 185 knots to 142 knots. At 0950:46, the controller instructed N7850P to extend his left downwind leg and to follow the Gulfstream. The pilot of N7850P acknowledged extending his left downwind leg and that he would be number two. At 0951:47, the controller cleared N534QS to land on runway 3. At 0951:53, the controller instructed N7850P to report when he had the Gulfstream in sight, and that it had just passed right to left ahead of him on base leg; there was no reply from the accident pilot. At 0952:05, the controller advised the accident pilot that the Gulfstream was now ahead and to his left, eleven o'clock and 2 miles, left base to final. At 0952:12, the accident pilot replied (first part unintelligible), "…blue Gulfstream, sun's in my eyes." At 0952:43, the controller advised the accident pilot that the Gulfstream was off to his left and on final; the accident pilot responded, "Gulfstream on final." At 0953:09, the controller asked the accident pilot to confirm that he had the Gulfstream in sight; the pilot responded that the Gulfstream was in sight at 0953:12. At 0953:36, the controller advised the pilot of N7850P to standby for a possible go-around, to which the pilot confirmed. At 0954:06, the controller instructed the accident pilot to start a climb and go around. At 0954:06, an unidentified pilot radioed to the controller that there was an airplane on final that just went down. There were no further communications received from N7850P. The following data reveals the horizontal and vertical separation between the two airplanes over the next 15 seconds: 0952:45 0.80nm 300 feet 0952:50 0.58nm 300 feet 0952:55 0.42nm 300 feet 0953:00 0.23nm 300 feet This data revealed that the Gulfstream was always higher than the Cirrus on the approach. The data further indicates that about 0953:06, N534QS passed over top of N7850P by approximately 300 feet. At this point the distance between the Gulfstream and Cirrus steadily increased. About 0953:12, the Gulfstream was about 0.11 nm ahead of and 200 to 300 feet higher than N7850P on final. N7850P was about 300 feet below the Gulfstream for most of the final approach to runway 3. The last radar return from N7850P at 0954:02, showed the airplane at an altitude of 1400 feet above ground level. The Gulfstream had passed that location approximately 30 seconds earlier and 150 feet higher than N7850P. The IIC recorded comments from several witnesses to the accident. One witness reported that she observed an aircraft at an angle and that it fell flat to the ground. A second witness stated that an aircraft went approximately 100 feet over houses then started a turn and went down toward the houses; it was lower than normal. Another witness reported that he saw the Gulfstream go overhead, then looked back and observed [the accident airplane] very low, saw it bank left about 100 degrees from the original direction that it was heading, then lost sight of it as it went behind a building, and then heard it crash. He added that it was very close behind the Gulfstream. A fourth witness reported seeing an aircraft coming from the southwest headed towards the school, very close to the ground, and it flipped on its side in the air. It then flipped back around and started to nose dive toward the ground. The airplane was recovered from the front yard of the private residence and examined. Fire-damaged components (primary flight and multifunction electronic displays) that contained non-volatile memory were removed from the instrument panel. These components were sent to the National Transportation Safety Board's Vehicle Recorder Division in Washington, D.C., for examination. PERSONNEL INFORMATION The pilot, age 62, held a private pilot certificate, which was issued on October 6, 2004, with an airplane single-engine land rating. His most recent Federal Aviation Administration (FAA) first-class airman medical certificate was issued on March 31, 2010, at which time he reported a total flight time of 700 hours. The certificate revealed the limitation "holder shall possess glasses for near and intermediate vision." A damaged pilot's logbook was recovered from the accident site. The logbook covered dates from November 14, 2009 to December 9, 2010. A further review of the logbook revealed that there were no totals forwarded from previous logbooks, and the times logged were exclusively for N7850P. It was observed that about 62 hours of logged flight time in the accident airplane had been recorded in the recovered logbook. It was also observed that the vast majority of those flights logged were flights been between SOW and SDL. AIRCRAFT INFORMATION The airplane, a Cirrus SR22-1351, received its standard airworthiness certificate on March 17, 2005. It was equipped with an S-TEC 55X autopilot, Avidyne Entegra Primary and Multifunction Flight Display (PFD, MFD), dual Garmin GNS 430s, GPS navigation transceivers, as well as an engine monitor, and XM satellite weather interface. One of the pilot's logbook entries was labeled "Annual Service" and dated June 26, 2010, at a Hobbs time of 621.9. No maintenance records were obtained during the investigation. METEOROLOGICAL INFORMATION At 0953, the SDL weather reporting system, located about 1 nm from the accident site, reported wind 250 degrees at 4 knots, visibility 10 miles, temperature 8 degrees Celsius (C), dew point 4 degrees C, and an altimeter setting of 30.18 inches of mercury. A senior NTSB meteorologist reported that astronomical data from the United States Naval Observatory located in Washington, D.C. revealed that on December 15, 2011, Sunrise was at 0724 MST. The meteorologist added that at 0954 MST, the Sun was 23.1 degrees above the horizon at an azimuth of 143 degrees true, or off of the right wing of the accident airplane, given his heading of 222 degrees magnetic, as reported by the IIC. WRECKAGE AND IMPACT INFORMATION The airplane came to rest about 0.75 miles from the threshold of runway 3 at SDL, and in the front yard of a residence at an elevation of 1,417 feet mean sea level. The debris field indicated that the energy path was oriented on a heading of about 275 degrees magnetic. The airplane came to rest on a measured magnetic heading of 232 degrees. The main wreckage came to rest about 80 feet from the initial point of impact and consisted of the entire fuselage and carry-though wing, minus various smaller components found in the debris field. The initial point of impact was a 7-foot tall hedge located on the adjacent neighbor's property that was missing the top portion of its branches. The driveway the hedge abutted to had a steel gate that exhibited impact damage and white paint transfer marks. The gate was observed separated from its hinges and lying in the street. The right wingtip of the accident airplane came to rest in the driveway near the gate and white paint transfer marks were present across the cement driveway. One black transfer mark was noted on the edge of the driveway, and the hedge between the two properties was damaged. A shallow trench was observed which contained the front nose landing gear strut, nose wheel assembly, and other small pieces of airplane debris leading away from the hedge on the side opposite the driveway leading towards the main wreckage for about 15 to 20 feet. The engine and propeller remained attached to the firewall with portions of the upper and lower cowlings still attached to each other. Fire consumed most of the roof and right side of the fuselage. The cockpit area exhibited extensive fire damage from the fire wall aft to the bulkhead aft of the Cirrus Airframe Parachute System (CAPS) enclosure. The empennage remained attached to the fuselage and exhibited extensive thermal damage. The right side of the wing from the cuff outboard was consumed by fire. The right flap and right aileron were mostly consumed by fire, and the identifiable portions of each had come to rest behind the wing. The left wingtip was observed separated and was located under the right side of the horizontal stabilizer. The left side of the wing exhibited impact damage. The fuel cap was present and secure. A stick was inserted in the fuel tank. From the bottom lip of the filler cap to the bottom of the tank the stick measured roughly 18 centimeters; when the stick was extracted from the tank, 16 centimeters of the stick was observed to be wet. The wing lay relatively flat but slightly tipped forward. The left flap and aileron remained attached to the wing and exhibited impact damage. Aileron control cable continuity was verified. The roll trim actuator was in between neutral and full left trim. The flap actuator shaft was extended approximately one half inch from the actuator housing, which was consistent with a flap setting of 100 percent, or fully extended. The vertical stabilizer remained attached to the empennage and exhibited impact and fire damage. The rudder remained attached to the vertical stabilizer and exhibited impact damage. Rudder control cable continuity was verified. The horizontal stabilizer remained attached to the empennage and exhibited impact and fire damage. The left and right elevators remained attached to the horizontal stabilizer. Elevator control cable continuity was verified. The pitch trim actuator was in an approximate neutral position. The right crew door was separated from the fuselage and exhibited fire and impact damage. The left crew door remained attached to the fuselage at the lower hinge and exhibited fire and impact damage. The baggage door remained attached to the fuselage and exhibited fire and impact damage. The nose landing gear assembly separated from the engine mount. The right main landing gear remained attached to the wing and exhibited impact and fire damage. The left main landing gear separated from the wing and was located about 25 feet aft of the main wreckage near the left wheel pant. The Cirrus Aircraft Parachute System (CAPS) safety pin was located on the bolster switch panel below the ignition switch. A grommet with red material consistent with the Remove Before Flight tag was present on the key ring style retainer containing the safety pin. The CAPS activation handle, handle holder, and mounting bracket were not observed. The activation cable housing was mostly consumed by fire, with only the wire mesh having been left behind on the activation cable. The activation cable was present and attached at the igniter. The other end of the activation cable had a ball swage on it but no activation handle. The CAPS enclosure cover remained attached to the left fuselage half and exhibited fire damage. The only anomaly noted during the engine examination was a reddish colored residue on the forward half of the piston head and around the forward half of the intake valve face on the #1 cylinder. The propeller remained attached to the engine and exhibited impact damage. The spinner had deformation on one side between two of the propeller blades. All three propeller blades were bent aft. Two of the propeller blades had scratches spanwise and chordwise on the cambered side. MEDICAL AND PATHOLOGICAL INFORMATION An autopsy was performed on the pilot at the Maricopa County Office of The Medical Examiner, Phoenix, Arizona, on December 16, 2011. The cause of death was reported as "Thermal burns." The FAA's Civil Aerospace Medical Institute performed forensic toxicology on specimens from the pilot. The report stated no carbon monoxide and no cyanide was detected in the Blood, no ethanol detected in the Vitreous, and 12.39 (ug/ml, ug/g) Acetaminophen detected in Urine. TESTS AND RESEARCH The NTSB IIC retained custody of the PFD and MFD. Both components were shipped to the NTSB Vehicle Recorder Laboratory In Washington, D.C. for examination and analysis by a vehicle recorder specialist who reported the following: PFD The PFD was damaged by impact forces and fire. The circuit card which contained the 2 Flash memory chip was extracted from the damaged housing and placed in a surrogate PFD unit for download. The PFD contained approximately 17 hours of flight data, including the accident flight. MFD The exterior of the MFD unit was damaged by fire. However, the MFD card was undamaged and data was recovered normally. The specialist reported that a review of the recovered data revealed that the flight departed SOW at 0913 and climbed to a cruise altitude of 8,400 feet. Between 0932:13 and 0940:00, no data was recorded on the PFD; this is a known behavior with this version of PFD software. At 0940:20, the airplane began its descent at approximately 1,000 feet per minute (fpm). At 0954, the airplane experienced an upset, rolling rapidly from 35 degrees left wing down to over 77 degrees left wing down, before rapidly rolling to 25 degrees right wing down. At this time the airplane's rate of descent was in excess of 3
The pilot's failure to maintain adequate separation behind a corporate jet, which resulted in an encounter with wake turbulence and a subsequent loss of control.
Source: NTSB Aviation Accident Database
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