Panoche, CA, USA
N364AB
BEECH B36
The pilot was delivering the single engine airplane from England to the west coast of the United States. According to his resume, he had piloted 196 Atlantic crossings in general aviation airplanes. The trip began about 1 week before the accident. The flights from England to Maine, with a pilot-rated passenger on board, consisted of 6 legs, with a total flight time of about 27 hours over a period of about 96 hours. The passenger and pilot separated in Bangor, Maine, and the pilot continued to Kentucky that same day, with an additional 2 legs and 6 hours flight time. He spent a total of 13 hours on the ground in Kentucky before departing early in the morning on the day of the accident. The first leg was 5 hours followed by a fuel stop. The next leg was 3 hours 20 minutes, and another fuel stop was made. The pilot then departed on the accident leg to his destination in California. The pilot flew the over 4-hour accident leg under visual flight rules using air traffic control flight following services. He flew directly between waypoints instead of on established airways. The airplane was equipped with a panel-mounted GPS unit with altitude information capability, and the pilot's iPad was equipped with current flight planning and guidance software, and electronic navigation charts. The pilot had access to sufficient information in flight to remain clear of terrain, but the investigation was unable to determine whether the pilot accessed that information during any part of that flight leg. When the airplane was about 65 miles from its destination, the pilot began a steady descent from his cruise altitude of 12,500 feet, which he had flown without supplemental oxygen. The destination elevation was 230 feet. Due to coverage limitations, radar contact with the airplane was lost when it was descending through 5,100 feet. At this point, the airplane was 46 miles from its destination, and the controller cancelled the flight-following services. There were no further communications from the pilot; up to this point, he had acknowledged all transmissions from ATC. Twelve miles after flight-following services were cancelled, the airplane impacted a hillside at an elevation of about 1,960 feet. Ground scar and wreckage information indicated that the airplane impacted in a wings-level attitude on a near-horizontal flight path. The airplane was highly fragmented and damaged by postimpact fire. Evidence was consistent with the landing gear and flaps retracted. Postaccident examination of the airframe and engine revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation. Darkness prevailed at the time of the accident, and AIRMETs for mountain obscuration were current for the time and location of the accident. Satellite and weather radar data suggested the presence of instrument meteorological conditions along parts of the airplane's route, but the investigation was unable to determine whether the pilot encountered or entered instrument meteorological conditions during the descent. Extrapolation of radar-derived speed and descent rate data indicated that the airplane descended steadily on track from cruise to the impact point. The pilot's autopsy indicated that the cause of death was multiple blunt trauma injuries, with no adverse pre-existing conditions. The effects of possible fatigue or hypoxia on the pilot's performance could not be determined.
HISTORY OF FLIGHT On March 14, 2012, about 1955 Pacific daylight time (PDT), a Beech B36TC, N364AB, was substantially damaged when it impacted terrain in the Diablo Mountain range near Panoche, California, during a delivery flight from Gloucester, England, to San Jose, California. The airplane was recently purchased and operated by Lafferty Aircraft Sales (LAS), and was operated by American King Air Services (AKAS). The pilot sustained fatal injuries. The accident leg of the flight was conducted under the provisions of 14 Code of Federal Regulations Part 91, and in accordance with visual flight rules (VFR). Darkness and possible instrument meteorological conditions prevailed, and no Federal Aviation Administration (FAA) flight plan was filed for the flight. According to the pilot-rated passenger who flew with him for a portion of the trip, the pilot took a commercial flight from South Carolina to Florida on March 7, 2012, and the two of them then flew commercially to London, England, that evening. They arrived in London on March 8, and began the delivery flight the next day. They landed in Bangor, Maine, on March 13, where the passenger separated and returned to Florida via commercial airline service. The pilot continued with the delivery flight, and made an overnight stop in Kentucky that evening. The pilot departed Kentucky about 0900 local time on March 14, made one fuel stop in Oklahoma, and a second in Arizona. During the Arizona fuel stop, the pilot informed his wife that his planned overnight stop was at Hollister Municipal Airport (CVH), Hollister, California, and that the route for the last segment of that flight was direct from the Palmdale very high frequency omnirange facility (PMD VOR) to CVH. By the morning of March 15, neither the wife nor the pilot's business partner had heard from the pilot, and they began attempts to contact him. The FAA issued an Alert Notice (ALNOT) for the missing airplane later that morning. About 1200 PDT on March 17, the wreckage was found on a hillside, located on a ground track between PMD and CVH. The wreckage was located on a steep slope, was highly fragmented, and was damaged or consumed by fire. All major airplane components, or elements from them, were identified at the accident site. The wreckage was recovered to a secure facility for additional examination. The passenger stated that they did not experience any mechanical anomalies during his trans-Atlantic portion of the trip. While at the fuel stop in Arizona, the pilot told his wife that the airplane was performing "perfectly." PERSONNEL INFORMATION The pilot was the president of AKAS, located in South Carolina. According to its website, one service provided by AKAS was the transport/delivery of airplanes over long distances. The pilot was transporting the airplane for LAS of San Jose, California. Records provided by the FAA and LAS indicated that the pilot held multiple certificates and ratings, including an Airline Transport Pilot certificate. The 78-year-old pilot reported a total flight experience of about 13,400 hours, including about 300 hours in Beech 35/36 airplanes. His most recent FAA second-class medical certificate was issued in October 2011. The pilot's resume reported that he had 196 Atlantic crossings in general aviation aircraft. According to persons knowledgeable about the pilot's flying habits, whenever possible, although he was instrument rated and current, the pilot preferred to fly under VFR, and via direct routes using GPS. Witness and tracking data from the flight indicated that the pilot's behavior and actions were consistent with his reported preferences. Details regarding the pilot's wake/sleep cycles and quality of sleep during the trip were not available. In September 2007, based on a telephone call from an unidentified woman, the FAA began an investigation into the pilot's fitness to hold a second-class medical certificate. The caller claimed that the pilot had significant vision and hearing deficiencies. In spring 2007, the FAA determined that the pilot remained qualified to hold that certificate, and the available evidence indicated that the complainant was the pilot's ex-wife. AIRCRAFT INFORMATION The airplane was manufactured in 1991, and was equipped with a Continental Motors TSIO-520 series engine. The most recent annual inspection was completed in England on March 9, 2012. The maintenance records indicated that at the time of that inspection, the airframe, engine, and propeller each had a total time in service of 1,302 hours. The records also indicated that about 20 discrepancies that were noted by the inspecting technicians were dispositioned as "owner requests no action," and therefore no corrective actions for those items were accomplished. The airplane was equipped, approved, and current for instrument flight rules (IFR) operations. In addition to the normal complement of avionics, the airplane was equipped with an autopilot and a King KLN-90B IFR certified GPS navigation system. METEOROLOGICAL INFORMATION On the day of the accident, accident locale sunset occurred at 1913, and local civil twilight ended at 1938. The moon did not rise until 0144 the next morning. AIRMETs for icing, IFR conditions, and mountain obscuration were current for the accident locale and flight altitudes. The investigation was unable to determine whether the pilot was aware of those AIRMETs. METARs from surrounding airports about the time of the accident were as follows: CVH (leg destination; ~34 nm northwest of accident, elevation 230 ft) 1945 PDT Wind 290 degrees at 7 knots, visibility 10 miles, few clouds at 1,400 ft agl, overcast at 3,000 ft agl, temperature 14 degrees C, dew point 12 degrees C 2005 PDT Wind 300 degrees at 5 knots, visibility 10 miles, overcast at 3,000 ft agl, temperature 14 degrees C, dew point 12 degrees C SJC (San Jose, ultimate destination; ~72 nm northwest of accident, elevation 62 ft) 1953 PDT Wind 100 degrees at 5 knots, visibility 10 miles, light rain, few clouds at 1,500 ft agl, scattered clouds at 3,000 ft agl, overcast at 6,500 ft agl, temperature 14 degrees C, dew point 12 degrees C SNS (Salinas, ~38 nm west northwest of accident, elevation 85 ft) 1953 PDT Wind 340 degrees at 6 knots, visibility 10 miles, light rain, overcast at 6,500 ft agl, temperature 16 degrees C, dew point 12 degrees C NLC (LeMoore, ~45 east southeast nm west northwest of accident, elevation 232 ft) 1956 PDT Wind 350 degrees at 8 knots, visibility 10 miles, scattered clouds at 6,500 ft agl, overcast at 15,000 ft agl , temperature 18 degrees C, dew point 8 degrees C Rawinsonde data (information derived from an instrument package ascending through the atmosphere) identified a saturated or near-saturated environment between about 3,300 and 8,200 feet mean sea level (msl). A cross-section of that data identified an extensive area of relative humidity values greater than 94 percent between near-surface altitudes and approximately 4,300 feet msl. Satellite imagery indicated that cloudy conditions dominated much of the accident region, but a layer of high clouds prevented determination of whether clouds were present along the airplane's flight path or at the flight elevations near the accident site. Doppler weather radar imagery did not indicate significant meteorological targets above the accident location between altitudes of 3,100 and 9,100 feet msl.AIDS TO NAVIGATION According to the pilot's business partner, the pilot wanted to ensure that the database in the KLN 90B GPS unit was updated for the United States before he began the flight, and the partner understood that that update had been accomplished. According to a representative of the manufacturer of the KLN 90B, the device includes altitude features such as Minimum Safe Altitudes, Minimum En route Altitudes and altitude alerting. The pilot also had a personal iPad with the "ForeFlight" program installed. The pilot-rated passenger who accompanied him from England to the US reported that the pilot used the iPad for that portion of the trip. The iPad was recovered from the wreckage and sent to the NTSB Recorders laboratory for download. The iPad/Foreflight does not store track data. The last map viewed in the ForeFlight program was that of the accident route leg, overlaid on IFR (instrument flight rules) low altitude en route charts. The accident leg route on the device was depicted as a straight line between the PMD VOR and CVH, the destination airport. Reconstruction of the flight route from England to the accident location, using commercial tracking vendor data and air traffic control radar data, revealed that the pilot primarily flew direct legs between origin and destination airports, as opposed to routes that used established airways and ground-based navigation facilities. The iPad/Foreflight examination results indicated that the pilot had the information necessary to enable him to determine the minimum safe altitudes for his route of flight and current location. A review of the applicable VFR Sectional chart revealed that the charted Maximum Elevation Figure (MEF) was 5,600 feet msl in the vicinity of the accident location. MEF values provide pilots with a ready means to ensure terrain clearance, and they range between 100 and 300 feet above the highest obstruction within a given quadrangle. A review of the applicable En route Low Altitude IFR chart revealed that the applicable OROCA (Off Route Obstruction Clearance Altitude) was 7,600 feet msl. CVH elevation was 230 feet msl. The airplane impacted terrain at an elevation of 1,960 feet msl. COMMUNICATIONS Flight Services Once in the US, the pilot did not file any flight plans, and did not obtain any official preflight weather briefings through Lockheed Martin Flight Services (LMFS), either telephonically or via the Internet. No records of any other pilot attempts to obtain weather information from other sources were located. The only contacts the pilot had with LMFS were two separate radio communications, approximately 1 hour apart, on the morning of the accident day. Both communications occurred while the airplane was airborne and inbound to Woodward, Oklahoma. In both of those communications, the pilot requested and was provided weather information for the West Woodward airport (WWR). Air Traffic Control The pilot operated the accident leg under VFR but was using air traffic control (ATC) flight following services. The last known ATC facility that the pilot was communicating with was the Oakland Air Route Traffic Control Center, normally referred to as "Oakland Center." He had been assigned a discrete transponder beacon code for flight following purposes, and was tracked on radar until shortly before the accident. Review of the communications revealed that about 1949, the pilot informed ATC that he would like to begin a descent if that was acceptable to them. The controller approved the descent, and instructed the pilot to "maintain VFR," to which the pilot responded "roger will do." The radar data indicated that the pilot vacated his cruise altitude of 12,500 feet, and established a steady state descent. About 1957, the controller asked the pilot to "report the Hollister area in sight," which the pilot agreed to do. About 13 seconds later, the controller told the pilot "you have descended below my radar coverage, radar contact is lost and I won't be able to see you again, you can contact NorCal approach in about ten miles on one two seven point one five for further advisories. And November four alpha bravo squawk V-F-R and frequency change is approved." The pilot asked the controller to repeat the frequency, which he did, and about 1958 the pilot confirmed the frequency. That was the last known communication from the airplane. WRECKAGE AND IMPACT INFORMATION On the morning of March 15, when neither the pilot's wife nor his business partner was able to contact the pilot, they notified the FAA. Later that morning the FAA issued an alert notice (ALNOT) that the airplane was missing, and review of communications and radar information enabled notification of authorities in the region of the last known location of the airplane. About 1130 on March 15, a deputy of the San Benito County Sheriff's department spied what he believed to be the wreckage. At that time, the deputy was positioned on a road several hundred feet below, and a few thousand feet laterally, from the wreckage. A search and rescue officer hiked up to the site, and confirmed that it was the airplane. The accident site was in remote, sparsely populated mountainous terrain, with sparse tree and shrub cover. The accident site was situated about 34 miles from the destination airport. The magnetic heading from the accident site to the destination airport was approximately 294 degrees, and the debris field axis was similarly oriented. Site elevation was approximately 1,960 feet above mean sea level (msl). The impact site was on a localized upslope of approximately 35 degrees, and was situated on the northwest side of a wider flat-floored valley. A straight-line projection from the impact site back on the reverse azimuth of the impact heading showed that the impact site was the highest terrain for at least one-half mile, and possibly significantly more. The debris field extended approximately 250 feet, but most of the debris was concentrated within about 60 feet of the initial impact point. Ground and vegetation scars were consistent with the airplane being approximately wings-level, in a level pitch attitude, at impact. Initial ground contact occurred with the right wingtip, which created a 15 foot long cut in a steep but sandy hillside that was parallel to the impact heading. That ground scar indicated that the flight path angle was approximately level or slightly descending. The airplane was highly deformed and/or fragmented, and damaged or consumed by fire. All major components were accounted for at the accident site. The engine was partially attached to its mounts and firewall, and partially embedded in the slope. The propeller blades were separated from the engine and hub. One wing root remained partially attached to the fuselage lower structure. The fuselage/cabin was highly fragmented, and the bulk of it was consumed by fire. The vertical and right horizontal stabilizers were consumed by fire, and the left horizontal stabilizer was intact but separated from the airplane. In addition to the on-scene examination of the wreckage, the recovered airframe and engine were examined at the recovery facility several weeks later. All observed fire damage was consistent with an on-ground (stationary) post impact fire. The observed evidence was consistent with landing gear and flaps retracted, and engine/propeller operating normally, at impact. No evidence of any pre-impact mechanical malfunction was noted during either examination. MEDICAL AND PATHOLOGICAL INFORMATION The Monterey County California Coroner's office conducted an autopsy on the pilot. The autopsy report indicated that the cause of death was "multiple blunt force injuries." The pilot also sustained post-mortem thermal injuries. The FAA Civil Aeromedical Institute conducted forensic toxicology examinations on specimens from the pilot, and reported that no ethanol, or any screened drugs, were detected. ADDITIONAL INFORMATION Trip Chronology Witness and flight tracking data enabled the re-creation of the trip chronology. The pilot left his home in South Carolina on Wednesday, March 7, via a commercial flight. Later that evening he and the passenger took a commercial flight from Miami, Florida, to London, England, arriving in London about noon on Thursday, March 8. They then traveled by bus to Gloucester, England, where the airplane was located. The passenger, who accompanied the pilot back to the United States, reported that the trip from London to Gloucester appeared to be "longer and more difficult than the pilot expected." The original plan was to depart Gloucester for Wick, Scotland, later that day, but paperwork issues delayed their departure until early Friday afternoon. They overnighted in Wick. The total flying time on Friday was about 3 hours. Their
The pilot’s lack of situational awareness regarding the surrounding terrain while descending during dark night conditions, which resulted in controlled flight into terrain.
Source: NTSB Aviation Accident Database
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