Breckenridge, TX, USA
N14HP
GRUMMAN F8F-1
A witness to the accident reported that the pilot announced over the radio that he was going to perform a half Cuban eight aerobatic maneuver after takeoff and then overfly the runway in the opposite direction. The witness stated that, after takeoff, the airplane entered a shallow climb to about 150 feet before it pitched up into a near vertical climb. The airplane continued the climb in an inside loop before leveling out, inverted, about 500 feet above the runway, heading in the opposite direction of the takeoff. The witness then saw the airplane's wings roll suddenly before the airplane entered a near-vertical descent. The witness described the final portion of the aerobatic maneuver as a split-S maneuver, or a descending half loop, from which the airplane did not recover before colliding with trees and terrain on a southeasterly heading. The witness stated that the airplane exploded on impact and that a postimpact fire ensued. The postaccident examination of the airplane revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. The pilot reportedly was as an experienced aerobatic pilot who had routinely performed at airshows throughout his flying career. The pilot's medical history included coronary artery and peripheral vascular disease, cataract surgery, and hypothyroidism. The autopsy was limited by the absence of most of the cardiac tissue; therefore, it could not be determined if the pilot was impaired or incapacitated by an acute coronary event during the low-altitude aerobatic maneuver.
HISTORY OF FLIGHTOn April 4, 2012, at 1410 central daylight time, a Grumman model F8F-1 airplane, N14HP, was substantially damaged when it collided with trees and terrain during a low-altitude aerobatic maneuver performed shortly after takeoff from the Stephens County Airport (BKD), Breckenridge, Texas. A postimpact fire ensued. The commercial pilot was fatally injured. The airplane was registered to and operated by the Breckenridge Aviation Museum under the provisions of 14 Code of Federal Regulations Part 91 without a flight plan. Day visual meteorological conditions prevailed for the personal flight that was originating at the time of the accident. A witness to the accident reported that he was in his airplane preparing to depart when the accident airplane was taxiing toward runway 17. He told the accident pilot, via radio, that he wanted to watch the accident airplane takeoff ahead of him. The accident pilot reportedly announced over the radio that he was going to perform a Half Cuban Eight aerobatic maneuver after takeoff and then overfly the runway in the opposite direction. The witness stated that after takeoff the accident airplane climbed about 150 feet in a shallow climb before it pitched-up into a near vertical climb. The airplane continued the climb in an inside loop before leveling out, inverted, about 500 feet above the runway, heading in the opposite direction of the takeoff. The witness then saw the airplane's wings roll suddenly before the airplane entered a near vertical descent. The witness described the final portion of the aerobatic maneuver as a split-S maneuver, or a descending half loop, from which the airplane did not recover before impacting the terrain on a southeasterly heading. The witness stated that the airplane exploded on impact and a postimpact fire ensued. Another witness reported seeing the airplane pitch-up into a steep climb shortly after takeoff. The airplane continued in the steep climb to about 1,000 feet above the runway where it entered a right descending roll. The witness stated that the airplane was rolling toward wings level when it descended into trees located off the south end of runway 17. The witness noted that the airplane appeared to be recovering from a dive when it impacted terrain. PERSONNEL INFORMATIONAccording to Federal Aviation Administration (FAA) records, the pilot, age 77, held a commercial pilot certificate with single and multi-engine land airplane and instrument airplane ratings. His last aviation medical examination was completed on June 24, 2011, when he was issued a second-class medical certificate with a restriction for near vision corrective lenses. The most recent pilot logbook entry was dated April 2, 2012. At that time, the pilot had accumulated 16,689.4 hours total flight time, of which 16,227.2 hours were logged as pilot-in-command. He had logged 10,498.2 flight hours in single-engine airplanes and 6,191.2 hours in multi-engine airplanes. He had accumulated 805.1 hours in actual instrument conditions, 895.0 hours in simulated instrument conditions, and 681.3 hours at night. The logbook contained a summary of his flight experience in numerous aircraft types, including the accident airplane make/model. According to the summary, he had logged 10,045.4 flight hours in warbird classification airplanes, including 2,007.8 hours in Grumman airplane models F8F-1 and F8F-2. He had logged 288.0 hours in the past year, 138.3 hours in the prior 6 months, 58.7 hours in the previous 90 days, and 27.5 hours in the last 30 days. The pilot did not log a flight within 24 hours of the accident. The pilot's last flight review was completed on March 8, 2011, in a Beechcraft model B60 airplane. The pilot reportedly was as an experienced aerobatic pilot who had routinely performed at airshows throughout his flying career. AIRCRAFT INFORMATIONThe accident airplane was a 1945 Grumman model F8F-1, serial number (s/n) 90446. A 2,100-horsepower Pratt & Whitney model R-2800-34W reciprocating engine, s/n P333510, powered the airplane. The airplane was equipped with a constant speed, four blade, Aeroproducts model A-642-G1 metal propeller. The tail wheel-equipped airplane was configured with a single seat. It had a maximum takeoff weight of 8,800 pounds and was certified for aerobatic flight. The accident airplane was a flying museum-quality, World War II-era airplane, owned and operated by the Breckenridge Aviation Museum, Breckenridge, Texas. The airplane was used predominately as a static display museum attraction. However, the airplane was also flown at airshows around the United States that featured World War II-era airplanes. On May 22, 1987, the FAA issued the airplane a special airworthiness certificate, limited category, for exhibition purposes. The airframe had accumulated a total service time of 2,759.6 hours at the time of the accident. The last annual inspection was completed on March 22, 2012, at 2,758.7 total airframe hours. The engine had accumulated 133.3 hours since its last major overhaul, which was completed during January 2008. The propeller had accumulated 440.9 hours since it last overhaul, which was completed during April 2002. METEOROLOGICAL INFORMATIONAt 1415, the airport's automated surface observing system reported: wind 280 degrees at 8 knots, sky clear, visibility 10 miles, temperature 21 degrees Celsius, dew point 7 degrees Celsius, altimeter setting 29.88 inches of mercury. AIRPORT INFORMATIONThe accident airplane was a 1945 Grumman model F8F-1, serial number (s/n) 90446. A 2,100-horsepower Pratt & Whitney model R-2800-34W reciprocating engine, s/n P333510, powered the airplane. The airplane was equipped with a constant speed, four blade, Aeroproducts model A-642-G1 metal propeller. The tail wheel-equipped airplane was configured with a single seat. It had a maximum takeoff weight of 8,800 pounds and was certified for aerobatic flight. The accident airplane was a flying museum-quality, World War II-era airplane, owned and operated by the Breckenridge Aviation Museum, Breckenridge, Texas. The airplane was used predominately as a static display museum attraction. However, the airplane was also flown at airshows around the United States that featured World War II-era airplanes. On May 22, 1987, the FAA issued the airplane a special airworthiness certificate, limited category, for exhibition purposes. The airframe had accumulated a total service time of 2,759.6 hours at the time of the accident. The last annual inspection was completed on March 22, 2012, at 2,758.7 total airframe hours. The engine had accumulated 133.3 hours since its last major overhaul, which was completed during January 2008. The propeller had accumulated 440.9 hours since it last overhaul, which was completed during April 2002. WRECKAGE AND IMPACT INFORMATIONA postaccident investigation was completed by FAA Inspectors assigned to the Lubbock Flight Standards District Office (FSDO). The FAA on-site investigation confirmed that all airframe structural and flight control components were located at the accident site. The initial impact was located in a field about 1/2 mile south of the runway 17 departure threshold. The initial impact crater contained one propeller blade. The right wing had separated from the fuselage and was located about 25 yards south of the initial impact point. The main wreckage, which consisted of the fuselage, left wing, and empennage, was found entangled within trees about 35 yards southeast of the initial impact point. The engine was located about 100 yards south of the initial impact point. The propeller hub had separated from the engine and the propeller blades exhibited blade-twisting. All observed structural component failures were consistent with overstress separation. Flight control continuity could not be established between the individual flight control surfaces and their respective cockpit controls due to damage; however, all separations were consistent with overstress. The flap position could not be determined due to impact damage. The fuselage, including the cockpit and instrument panel, was fragmented and damaged by fire. The postaccident examination of the airframe, engine, and propeller revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. ADDITIONAL INFORMATIONFederal Aviation Regulation 91.303 required that aerobatic flight be conducted above 1,500 feet above ground level unless a specific waiver has been granted. According to FAA documentation, an aerobatic waiver had not been approved for flights over BKD. The Lubbock FSDO received a request for an aerobatic box in 2009, but a request for additional information made to the requester was not fulfilled and the request was not approved. MEDICAL AND PATHOLOGICAL INFORMATIONOn April 5, 2012, an autopsy was performed on the pilot at the Tarrant County Medical Examiner's District Morgue, located in Fort Worth, Texas. The cause of death for the pilot was attributed to multiple blunt-force injuries sustained during the accident. The autopsy report indicated that a majority of the heart and brain were not available for examination and that the degree of injury to the extremities precluded further evaluation of those areas. The FAA Civil Aerospace Medical Institute (CAMI) in Oklahoma City, Oklahoma, performed toxicology tests on samples obtained during the pilot's autopsy. No carbon monoxide or cyanide was detected in blood samples. Ethanol was detected in blood and liver samples, but was attributed to sources other than ingestion. Rosuvastatin was detected in liver and blood samples. Rosuvastatin, brand name Crestor, is a medication to treat high cholesterol and prevent heart disease. According to FAA medical documentation, the pilot reported having cataract surgery to his Aviation Medical Examiner (AME) in 2001. In March 2004, he requested a waiver for that procedure although he had already been granted a second class certificate in 2001, 2002, and 2003. In June of 2004 he reported a preoperative physical and a second cataract surgery (on the other eye). His second class certificate was issued routinely in 2004, 2005, and 2006. In 2007, the pilot reported having high cholesterol that was managed with Zetia and Crestor (ezetimibe and rosuvastatin, both cholesterol lowering agents). In 2008, the pilot reported the use of levothyroid (levothyroxine, thyroid hormone replacement). His second class certificates were issued by the AME on each of these visits. In 2009, per the FAA record, the pilot provided his AME results of a pharmacologic nuclear stress test along with results of cholesterol and thyroid testing. All were results were classified as being "normal." The FAA record also included a copy of a physician note from the pilot's cardiologist made during an office visit on May 14, 2010. In this note, the diagnoses included hyperlipidemia, coronary atherosclerosis of native coronary artery, peripheral vascular disease, and hypertension. The past history section detailed a PTCA (percutaneous transluminal coronary angioplasty) with stent placement of the right coronary artery and a PTA (percutaneous transluminal angioplasty) with stent placement in the popliteal artery. Laboratory results from the May 14, 2010, office visit indicated that the pilot had an elevated glucose level and normal cholesterol and thyroid hormone levels. In June 2010, the AME noted the laboratory results but did not comment on the recorded historical elements and issued a second class medical certificate. The FAA medical record also contained reports of an echocardiogram, another nuclear stress test, and a carotid Doppler examination being completed during 2011. The results of these tests were reported as being "normal" and the pilot was issued a second class medical certificate from his AME on June 24, 2011.
The pilot's loss of airplane control during a low-altitude aerobatic maneuver.
Source: NTSB Aviation Accident Database
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