Aviation Accident Summaries

Aviation Accident Summary ERA12CA275

Ruleville, MS, USA

Aircraft #1

N51037

AIR TRACTOR INC AT-602

Analysis

The pilot departed on an aerial application flight with an estimated 53 gallons of fuel. He had not reset the fuel totalizer before departure. He made numerous passes over a 100-acre field spraying fertilizer during the 30 minute flight. After his last pass, the pilot noticed a fuel flow fluctuation. The engine subsequently lost power at an altitude of 75 to 100 feet above the ground, and the pilot made a forced landing. He pulled the airplane off the ground again briefly to clear an obstruction; however, when the airplane touched down again, the left main landing gear sank into soft ground and sheared off. The airplane rotated to the right onto its nose, and the left wing sustained structural damage. Postaccident examination revealed that the left and right main fuel caps had a tight seal and there was no evidence of streaking or venting of fuel on the airplane or on the ground. The left, right, header, and purge fuel tanks were drained and yielded about 34 total ounces of fuel—two ounces from the right fuel tank and 32 ounces from the header tank. The left and purge tanks contained no fuel. No preaccident mechanical malfunctions or failures were found that would have precluded normal operation.

Factual Information

The pilot departed on an aerial application flight with an estimated 53 gallons of fuel. He had not reset the Shadin fuel totalizer prior to departure. He made numerous passes over a 100 acre field spraying fertilizer. On his last swath run he noticed the fuel flow fluctuate as he started a climb between 75 to 100 feet above ground level. The engine quit and he made a forced landing on a turn road. He observed a standpipe and attempted a lift off to clear the obstruction. The airplane touched down and the left main landing gear sank into soft ground shearing off the landing gear. The airplane rotated to the right onto its nose and back to the left. The left wing sustained structural damage. The total flight time was 30 minutes. The manufacture stated in an email to the NTSB investigator that the fuel burn rate at maximum takeoff power is 89 gallons per hour and the unusable fuel is 6 gallons. Post accident examination of the airplane by an FAA Inspector revealed the left and right main fuel caps had a tight seal. There was no evidence of streaking or venting of fuel on the airplane or on the ground. The fuel caps were removed and no fuel was present. The right fuel tank was sumped and about two ounces of fuel was drained from the fuel tank. The left fuel tank was sumped and no fuel was drained from the fuel tank. The header tank was sumped and about one quart of fuel was sumped from the header tank. The purge tank was sumped and no fuel was present.

Probable Cause and Findings

The pilot's inadequate preflight planning and in-flight fuel management, which resulted in a total loss of engine power due to fuel exhaustion.

 

Source: NTSB Aviation Accident Database

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