Los Lunas, NM, USA
N904DB
BLACK DONALD COZY III
While taxiing after landing, the engine lost power, and the pilot turned the airplane off the runway. The pilot exited the airplane and noticed smoke at the rear of the airplane near the engine. The pilot attempted to extinguish the fire; however, his efforts were unsuccessful, and the airplane was consumed by the fire. At the time of the accident, the airplane had accumulated 4.9 flight hours. Postaccident examination of the airplane found loose B-nuts on two fuel lines and one oil line. An oil streak was noted on the runway surface, and no oil was found in the engine. The pilot stated that the fire likely resulted from oil leaking onto the hot turbocharger.
While taxiing after landing, the engine lost power and the pilot turned the airplane off the runway. The pilot exited the airplane and noticed smoke at the rear of the airplane near the engine. The pilot attempted to extinguish the fire; however, his efforts were unsuccessful and the airplane was consumed by the fire. At the time of the accident, the airplane had accumulated 4.9 flight hours. Post accident examination of the airplane showed loose B-nuts on two fuel lines and one oil line. An oil streak was noted on the runway surface and no oil was found in the engine.
A loose oil line, which allowed oil to leak onto the hot engine turbocharger and resulted in a fire.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports