Aviation Accident Summaries

Aviation Accident Summary CEN13FA006

Mabank, TX, USA

Aircraft #1

N32GP

BEECH A36

Analysis

The pilot obtained a weather briefing the day before the accident; however, no record was found indicating that he obtained an updated briefing on the day of the flight, which would have included weather advisories for instrument meteorological conditions (IMC) surrounding the airplane's route of flight. After encountering low clouds at the destination airport, the pilot requested a clearance to divert to another nearby airport, and he was provided the clearance. No further radio transmissions were received. The airplane crashed between the two airports. Photographs of the flight conditions taken by a pilot flying in the area about the time of the accident showed low, overcast clouds above the airplane. A review of logbook entries and mechanic's statements did not reveal any unresolved maintenance or airworthiness issues. A postaccident examination of the wreckage revealed no preimpact mechanical malfunctions or failures that would have precluded normal operation. Propeller and internal engine components exhibited damage consistent with the production of power at the time of the accident. Therefore, on the basis of the evidence, the pilot most likely lost control of the airplane while maneuvering in IMC.

Factual Information

HISTORY OF FLIGHTOn October 6, 2012, about 0945 central daylight time, a Beech A36 airplane, N32GP, impacted terrain during a descent near Mabank, Texas. The pilot, pilot rated passenger and two other passengers were fatally injured. The airplane's airframe and engine were destroyed. The airplane was registered to and operated by Palm-L Aviation LLC under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Instrument flight rules conditions (IFR) conditions prevailed for the flight, which operated on an activated IFR flight plan. The flight originated from the Northwest Regional Airport (52F), near Roanoke, Texas, about 0845, and was destined for the Athens Municipal Airport (F44), near Athens, Texas. The pilot obtained a Direct User Access Terminal Service weather briefing at 1526 on the afternoon prior to the flight. There were no records of any updated briefings on the morning of the flight. The airplane was based at 52F and witnesses saw the airplane depart from there between 0830 and 0900. According to a copy of the pilot's flight plan, the listed route of flight was direct from 52F to F44 and no alternate airport was entered. The listed departure airport, 52F, did not have Jet-A fuel service. However, both F44 and the Terrell Municipal Airport (TRL), near Terrell, Texas, have services that dispense Jet-A fuel. An IFR flight plan from F44 to the Fletcher Field Airport, near Clarksdale, Mississippi, was also on file. According to air traffic control (ATC) information received from the Federal Aviation Administration (FAA), the flight encountered low clouds at F44 and requested a clearance to TRL. The flight was provided the clearance to TRL and subsequently given a frequency change. The FAA's last reported radar return from the airplane was at 0944:23 at a pressure altitude of 2,900 feet. No further radio transmissions were received. PERSONNEL INFORMATIONThe pilot held a private pilot certificate, with an airplane single-engine land and instrument airplane ratings. The pilot's most recent FAA third-class medical certificate was issued on August 31, 2011. The medical certificate had a limitation for corrective lenses. At that time, he reported that he had accumulated 340 hours of total flight time and had accumulated no flight time during the six months prior to that application. The pilot recorded in his logbook that he had accumulated 568.5 hours of total flight time and had accumulated 219.5 hours in turbine-powered airplanes. An endorsement, dated May 18, 2012, indicated that the pilot had completed the training required for operating pressurized aircraft. Another endorsement, dated February 16, 2012, indicated that the pilot satisfactorily completed an instrument proficiency check. An endorsement for a current flight review was not located in the pilot's logbook. The pilot-rated passenger held a private pilot certificate with a single-engine land rating. His most recent FAA third-class medical certificate was issued on April 26, 2012. The medical certificate had a limitation for corrective lenses. At that time, he reported that he had accumulated 130 hours of total flight time and had accumulated no flight time during the six months prior to that application. AIRCRAFT INFORMATIONN32GP, a 1985-model Beech A36, serial number E-2230, was a low wing, single-engine, six-place monoplane, which had retractable tricycle landing gear. According to FAA airworthiness records, the airplane was powered by a Rolls Royce 250-B17C turbine engine, which was installed in accordance with a Soloy Conversions, Ltd., supplemental type certificate SA3523NM. The installation was approved on a major repair and alteration form dated July 3, 1986. The engine drove a Hartzell, three-bladed, all-metal, constant-speed propeller. An airplane logbook endorsement indicated the airplane had its last annual inspection completed on December 13, 2011. At that time, the airplane had accumulated 2,451.8 hours of total time and the engine accumulated 854 hours of total time. That endorsement entry also indicated that the engine accumulated 205.6 hours since overhaul and 205 cycles since overhaul. A review of logbook entries and mechanic's statements did not reveal any unresolved maintenance or airworthiness issues. METEOROLOGICAL INFORMATIONThe National Weather Service had issued an Airman's Meteorological Information advisory that was current at the time period of the accident for IFR conditions in the area surrounding the flight. At 0953, about 324 degrees and 17 miles from the accident site, the recorded weather at TRL was: wind 020 degrees at 10 knots; visibility 10 statute miles; overcast clouds at 600 feet; temperature 12 degrees C; dew point 9 degrees C; altimeter 30.16 inches of mercury. At 0935, about 149 degrees and 23 miles from the accident site, the recorded weather at F44 was: wind 020 at 7 knots; visibility 3 statute miles; present weather mist; sky condition overcast clouds at 500 feet; temperature 14 degrees C; dew point 13 degrees C; altimeter 30.12 inches of mercury. A pilot who was flying in the area about 15 nautical miles northeast of the accident site took pictures of the flight conditions present about 0950. The images exhibited low overcast clouds above the airplane. The pilot's images are attached to the docket material associated with this case. AIRPORT INFORMATIONN32GP, a 1985-model Beech A36, serial number E-2230, was a low wing, single-engine, six-place monoplane, which had retractable tricycle landing gear. According to FAA airworthiness records, the airplane was powered by a Rolls Royce 250-B17C turbine engine, which was installed in accordance with a Soloy Conversions, Ltd., supplemental type certificate SA3523NM. The installation was approved on a major repair and alteration form dated July 3, 1986. The engine drove a Hartzell, three-bladed, all-metal, constant-speed propeller. An airplane logbook endorsement indicated the airplane had its last annual inspection completed on December 13, 2011. At that time, the airplane had accumulated 2,451.8 hours of total time and the engine accumulated 854 hours of total time. That endorsement entry also indicated that the engine accumulated 205.6 hours since overhaul and 205 cycles since overhaul. A review of logbook entries and mechanic's statements did not reveal any unresolved maintenance or airworthiness issues. WRECKAGE AND IMPACT INFORMATIONThe airplane impacted a field about one-half nautical mile east of the intersection of Farm to Market Road 90 and Van Zandt County Road 2702. A debris path started at an egg-shaped impact depression that was about 12 feet long and about two feet deep. The wreckage path continued on an observed heading of about 300 degrees and extended about 200 feet. The airplane was fragmented along this path with a section of the fuselage coming to rest about 95 feet from the start of the depression and the engine coming to rest about 190 feet from the start of the depression. All major components of the airplane were accounted for at the accident site. All flight control cables were traced. All observed control cable separations had a broom straw appearance consistent with overload. The left and right wing flap jackscrew actuator measurements corresponded to a zero degree flap setting. The aileron trim actuator measurement was consistent with a neutral setting. The landing gear linkage position was consistent with retracted landing gear. The engine separated from the airframe. Debris, consistent with ingested dirt, was found in the engine's compressor section. Fuel was found in the fuel pump filter bowl. The fuel shutoff valve handle was separated from its valve housing and light could be seen through a valve housing end when a flashlight illuminated the other end. The propeller was separated from the engine. Two propeller blades remained attached to their hub and they exhibited chordwise abrasions. The separated blade exhibited S-shaped bending and chordwise abrasion. Both vacuum pumps were disassembled and their rotors exhibited impact damage. All vanes in both pumps were intact. The attitude indicator was disassembled and its gyro and cage exhibited rotational scoring. The emergency locator beacon was found within the wreckage debris and it was crushed. Due to impact damage, the total fuel on board the airplane at the time of the accident could not be confirmed. MEDICAL AND PATHOLOGICAL INFORMATIONAn autopsy was performed on the pilot at the Southwestern Institute of Forensic Sciences at Dallas. The cause of death was listed as blunt force injuries. The FAA Civil Aerospace Medical Institute prepared a Final Forensic Toxicology Accident Report on the pilot. The report was negative for the tests performed. TESTS AND RESEARCHAnnunciator Panels Two annunciator panels were retained and subsequently examined by a Chemist in the National Transportation Safety Board (NTSB) Materials Laboratory. The report showed that the filaments exhibited inconclusive findings. The report is appended to the docket material associated with this case. Search and Rescue Actions According to a NTSB National Resource Analyst, radio and radar contact with the aircraft was lost at 0944. The FAA issued an alert notice reporting loss of contact at 1022. The Air Force Rescue Coordination Center opened a search mission and engaged a Civil Air Patrol (CAP) radar analyst at 1135. The CAP analyst reported an initial radar position at 1319, but the analyst did not have access to all of the FAA radar data. In particular, the analyst did not have access to information from the airport surveillance radar located at Sachse, Texas, the closest radar site to the aircraft. Consequently, the initial position provided to search teams was incorrect. At 1834, the CAP informed the rescue coordination center that, based on radar data, "...they have strong reason to believe that the aircraft is within the area of Terrell, Texas..." and that CAP aircraft and ground teams were headed to the Terrell area. At about 1630, after being notified by the Investigator in Charge that the aircraft was still missing, an NTSB radar analyst joined a teleconference involving FAA personnel from Fort Worth Air Route Traffic Control Center, Fort Worth Approach Control, the Central Service Area Quality Control Group, and headquarters staff from the FAA Compliance Services group, who provide search and rescue support assistance to local ATC facilities upon request. When it became apparent that neither the FAA or the CAP had been able to review the Sachse radar site's data, the NTSB analyst asked to obtain the file. The radar file was provided by Fort Worth approach control at 1942. The NTSB analyst reviewed the information and determined a last known position for the missing aircraft by 1956. The information was provided to Fort Worth Center at 2008 for relay to a sheriff's helicopter involved in the search, and the wreckage was located about 2025 within 0.2 nautical miles of the last known position provided by the NTSB, which was approximately 10 miles southeast of the area being searched by CAP based on their earlier radar assessment not using Sachse data.

Probable Cause and Findings

The pilot's loss of airplane control while maneuvering in instrument meteorological conditions.

 

Source: NTSB Aviation Accident Database

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