Stotts City, MO, USA
N6BS
CESSNA 310
The pilot and the pilot-rated passenger originally planned to make several circuits in the traffic pattern to test the right engine, which recently underwent extensive maintenance, before repositioning the airplane to a nearby airport. However, the flight was delayed to make an adjustment to the propeller lever friction lock. Because of the delay, the pilots departed after the sun had set and decided to fly directly to the other airport, which did not have runway lights. While en route, the right engine began to lose oil pressure and lost total power, so the pilot shut the engine down and feathered the propeller. The pilot elected to return to the departure airport, but was unable to maintain altitude. The airplane impacted trees and a postimpact fire consumed most of the airplane. According to witnesses, the airplane's nose gear landing strut was flat before departure and the pilots agreed they would leave the landing gear extended for the flight. Witnesses who saw the airplane just before impact confirmed the landing gear was extended. Postaccident examination of the right engine revealed the oil filter adapter was not properly assembled or adequately secured to the engine. The mechanic who performed maintenance to the oil adapter admitted that he did not follow the manufacturer's instructions when reassembling the adapter and when installing it on the engine. As a result, the adapter came loose during flight, which resulted in a loss of oil. Based on the single-engine performance data provided by the airplane manufacturer, the airplane should have had a single-engine climb rate of about 166 feet per minute with the landing gear extended, assuming the airplane was properly configured and the operating engine was producing full power. Although the airplane did not have a current annual inspection, no mechanical malfunctions or failures were noted with the airplane or the left engine that would have precluded normal operation.
HISTORY OF FLIGHTOn November 4, 2012, approximately 1800 central standard time, N6BS, a twin-engine Cessna 310 airplane, was substantially damaged when it collided with trees and terrain near Stotts City, Missouri. The commercial pilot and the pilot rated passenger were fatally injured. The airplane was registered to and operated by the pilot rated passenger. No flight plan was filed for the flight that originated from the Monett Regional Airport (HFJ), Monett, Missouri, about 1735, and destined for a private airstrip in Miller, Missouri. Night visual meteorological conditions prevailed for the repositioning flight conducted under 14 Code of Federal Regulations Part 91. According to a pilot rated witness, the airplane's right engine was recently overhauled and the accident flight was the first flight after the new engine was installed. He said the pilots had originally planned to fly to Miller on November 2nd, but had to postpone the flight because the left main landing gear brake was "soft" during the engine run-up. In addition to the left main landing gear brake problem, the nose landing gear strut was also flat. According to the mechanic, who was hired to overhaul the engine, the pilot rated passenger asked him if he would fix the nose gear strut. The mechanic told him it would take at least a day to complete the repair. Since the owner planned to fly the airplane to Ohio later that week for a corrosion inspection; he told the mechanic he would have the gear fixed then. In the meantime, he would fly with the landing gear extended because he was concerned the gear would get stuck in the nose well. As a temporary fix, the mechanic used shop-air provided by the Monett Airport manager to inflate the nose gear strut. The witness stated that the flight was re-scheduled for November 4th and he met both pilots at the Monett airport around 1700. During the preflight inspection, the pilots noted the nose gear strut was flat again and there was another discussion about keeping the gear extended for the flight. The two pilots boarded the accident airplane, started the engines, and taxied toward the runway. The airplane stopped on the taxiway and the engines were run-up three or four times. He said the pilots then taxied back to the hangar and shut the engines down. The pilot exited the airplane and said the right propeller was not "feathering" and needed to be fixed. The passenger called the same mechanic and asked him if he could look at the problem. The mechanic arrived 30-40 minutes later and opened the right inboard cowling on the right engine. About five minutes later, the mechanic said they were, "Good to go." According to the mechanic, the pilot rated passenger called him at 1648 and told him that the right propeller control lever was not moving smoothly through its full range of travel. There was no mention that the propeller was not feathering. The mechanic said he was surprised that they were planning to do an engine flight test at night. About 30-40 minutes later he arrived at the Monett airport and opened up the right inboard cowling for the right engine. The mechanic asked one of the pilots to move the propeller control lever in the cockpit through its full range of travel. The mechanic said the arm on the propeller governor moved smoothly from stop to stop as the lever was moved. He told one of the pilots to adjust the friction lock for the lever, which eased the tightness of the lever. He also noticed the nose gear strut was flat again. The witness said he heard the pilot and passenger discussing if they should postpone the flight because it was getting dark. They were originally going to make a few circuits around the traffic pattern before they flew to Miller. However, since they were delayed they agreed to just fly to Miller. The pilots got back in the accident airplane; the pilot passenger sat in the front left seat and the pilot sat in the front right seat. Both engines started normally and the airplane taxied toward the runway where another long engine run-up on the taxiway was conducted, which included cycling the propeller several times. The witness also noted that only the airplane's beacon lights were turned on. The mechanic also observed the airplane before it departed and provided a similar account of the engine run-up. He also confirmed that only the beacon lights were turned on. After the accident airplane departed runway 18, the witness departed in another airplane and followed them to Miller, which was 24 miles north of Monett. The witness planned to fly the pilot and pilot rated passenger back to Monett after they dropped off the accident airplane. The mechanic said that he was surprised when he saw the airplane heading north toward Miller because he thought they were going to stay in the traffic pattern to test the engine. He then called his assistant, who lived at the private airstrip in Miller, and told him that the accident airplane was headed that way. In an interview, the assistant said he received a call from the mechanic at 1738. He was surprised that anyone would attempt to land on an unlighted grass airstrip at night. The assistant said that by the time he and his girlfriend walked over to the runway, he could see the airplane approaching from the west. Only the airplane's beacon lights were turned on and he could not tell if the landing gear were extended because it was too dark. The airplane was approximately 500 to-800 feet above the ground and in a level flying attitude. The assistant said both engines sounded normal and there was "nothing indicating any distress." The airplane then made a smooth right turn toward the south and maintained a constant altitude. As the airplane turned south, the assistant said he got a call from the owner of the airstrip asking if he would bring a fire extinguisher out to the airplane when it landed. The assistant said he grabbed a nearby extinguisher, but the airplane never returned. The witness said that after he departed Monett airport, he established communication with the other pilots via a common air-to-air traffic frequency and made visual contact with the accident airplane. While en route, noted that the accident airplane was not on course for the private airstrip. The pilot rated passenger asked if they were heading in the right direction and the witness said they needed to correct 20-30 degrees back to the left. Shortly after, the pilot rated passenger said that "fuel or oil" was coming out of the right engine. He asked the witness to arrange for a fire extinguisher to be available when they landed, which he did. A few minutes later, the pilot rated passenger asked the witness where the private airstrip was located, and the witness told him they were "right on top of it." The pilot rated passenger then said they were losing oil pressure and were returning to Monett, followed by, "We shut the engine down." The witness responded, "Ok, I'll follow you." At this time, the witness said the accident airplane was turning from crosswind to downwind approximately 800-900 feet above the ground over the private airstrip. The witness said he then flew up along the right side of the accident airplane and noted that there was no smoke or fire coming from the engine. The witness then trailed back and to the right. He could not recall if the landing gear were extended, but did recall that the light on the nose gear was turned on. According to the witness, when the accident airplane was approximately 1 mile south of the private airstrip, the passenger announced, "110 knots" over the radio frequency. About 30 seconds later, the passenger said they were having trouble gaining altitude followed by they were not able to maintain altitude. The passenger then asked the witness for a vector to Mount Vernon Airport. The witness responded that it was 127 degrees and 4 miles, and he turned the runway lights on for them. The passenger again informed the witness that they were not able to maintain altitude. The witness said he could see the airplane losing altitude and advised them that Interstate 44 was one mile ahead. The pilot then announced they were going to land on the interstate. The witness said the accident airplane continued to lose altitude. The passenger then said, "Oh my God, I think we are going to crash." This statement was followed by, "We're going to crash." The witness said he saw the light on the accident airplane's nose gear illuminate the trees in front of them. Then the nose of the airplane pitched up, rolled slightly to the right, and then pitched forward, followed by flames and a fireball. Several people on the ground also witnessed the accident. One witness stated that he was at his home located about 1 mile northeast of the accident site when he first heard the airplane. He ran out on to his porch and established visual contact with the airplane. The airplane was descending toward the south, and the wings were "rocking" side to side. He said a bright "spotlight" was turned on at the bottom of the airplane. The witness, who was a diesel engine mechanic, said it sounded like only one of the airplane's engines was running, but he could not confirm which engine. He described the sound of the engine as revving up and down as if the pilot was "jockey-ing" the throttle. There was no smoke or fire trailing behind the airplane. The airplane then "dropped down" toward trees and the "throttle went wide open." Finally, the airplane "leaned off to the side" and he heard the sound of the airplane impacting the trees followed by two explosions. The witness saw a large cloud of black smoke and immediately went to the accident site. A second ground witness stated that he was walking out of the woods after hunting about 6-7 miles north of the accident site when he saw two airplanes flying south and were about 100 yards apart from each other. He said there was no smoke or fire trailing either airplane and both had their lights turned on. The witness said the "airplane on the right" had a "very bright spotlight" turned on. Both airplanes were 500 feet or higher above the ground and he did not hear the engines. The witness said he could not see any landing gear because it was "too dark outside." Another ground witness stated he was driving in his truck about ¾-mile north of the accident site when he first heard and saw the airplane. He said it flew directly over-head and was heading due south approximately 600 feet above the ground. The witness said it was dusk, around 1800, but still light outside. He said the airplane was descending in level flight and "the engine" was revving up and down. There was no smoke or fire trailing the airplane. He did not see any lights on the airplane, and thought the landing gear was extended. He said the airplane disappeared out of his view behind a house and made a "hard right bank." The witness did not see the airplane impact terrain but did see a large fireball moments later. PERSONNEL INFORMATIONThe pilot held a commercial pilot certificate for airplane single and multi-engine land, and instrument airplane. He was also a certified flight instructor for airplane single and multi-engine land, and instrument airplane. In addition, he held an airframe and power plant (A&P) certificate. A review of his logbook revealed that as of October 6, 2012, he had a total of 3,299 flight hours; 411 hours in multi-engine airplanes, of which, 102 hours were in a Cessna 310. The pilot rated passenger held a private pilot certificate for airplane single-engine land, and instrument airplane. A review of his logbook revealed that as of September 28, 2012, he had a total of 1,621.8 hours; of which, all 10.6 hours of multi-engine time were in the accident airplane. AIRCRAFT INFORMATIONA review of the airplane's maintenance logbooks revealed the accident airplane did not have a current annual inspection as required by Federal Aviation Regulation (FAR) 91.409. The last annual inspection was completed on August 10, 2010, at a total time of 4,549.7 hours. In September 2011, the airplane's previous owner hired a mechanic based in Arkansas to perform an annual inspection. According to the mechanic, the airplane was unairworthy because the nose-jack point had collapsed into the belly of the airplane and "a lot" of corrosion was found in the forward cabin bulkhead. Two Federal Aviation Administration (FAA) inspectors from the Little Rock Flight Standards District Office also examined the airplane and concurred that the airplane was unairworthy. The mechanic entered the unairworthy items in the aircraft logbook and made an endorsement that the airplane was "safe" to be ferried back to Missouri with the "gear down only." The FAA issued the owner a "Special Flight Permit" for this flight on November 10, 2011. The passenger purchased the airplane in January 2012 and according to FAA records, was registered on April 2, 2012. At some point, the airplane was flown to Miami, Oklahoma, for an annual inspection. According to the aircraft logbook, on February 12, 2012, the mechanic that was hired to perform the inspection wrote, "No corrosion of significant airworthy found," but did observe "buckling caused by improper jacking not airworthy condition." According to the FAA, there were no records that a ferry permit was issued for the flight to or from Miami, Oklahoma. A review of both pilot's logbooks revealed the airplane was flown a total of 8 times after the last "Special Flight Permit" was issued in 2011. The mechanic, who was hired to overhaul the engine, said he talked to the pilot on November 2nd, before the first planned test flight regarding the work he had performed on the engine. The mechanic said he had the right engine logbook, yellow tags and the engine data plate spread out on the horizontal stabilizer for the pilot to review, since he was also a mechanic. However, he said the pilot never looked at the logbook. He told the pilot that he had not "signed off" on the overhaul and was waiting for some older components to be replaced in addition to the flight test. At that time, he planned to sign off the work as a repair only. The mechanic said that after they talked, he gave the pilot the logbook along with the yellow tags and engine data plate because the pilot said the pilot rated passenger, who owned the airplane, wanted to review them. After the accident, the mechanic turned over the airplane's remaining maintenance logbooks that he had in his possession. The right engine logbook was never located. METEOROLOGICAL INFORMATIONAt 1753, the automated weather report at Joplin Regional Airport (JLN), Joplin, Missouri, about 24 miles west of the accident site, was reported as wind from 120 degrees at 3 knots, clear skies, temperature 13 degrees Celsius, dewpoint 3 degrees Celsius, and a barometric pressure setting of 30.08 inches of mercury. AIRPORT INFORMATIONA review of the airplane's maintenance logbooks revealed the accident airplane did not have a current annual inspection as required by Federal Aviation Regulation (FAR) 91.409. The last annual inspection was completed on August 10, 2010, at a total time of 4,549.7 hours. In September 2011, the airplane's previous owner hired a mechanic based in Arkansas to perform an annual inspection. According to the mechanic, the airplane was unairworthy because the nose-jack point had collapsed into the belly of the airplane and "a lot" of corrosion was found in the forward cabin bulkhead. Two Federal Aviation Administration (FAA) inspectors from the Little Rock Flight Standards District Office also examined the airplane and concurred that the airplane was unairworthy. The mechanic entered the unairworthy items in the aircraft logbook and made an endorsement that the airplane was "safe" to be ferried back to Missouri with the "gear down only." The FAA issued the owner a "Special Flight Permit" for this flight on November 10, 2011. The passenger purchased the airplane in January 2012 and according to FAA records, was registered on April 2, 2012. At some point, the airplane was flown to Miami, Oklahoma, for an annual inspection. According to the aircraft logbook, on February 12, 2012, the mechanic that was hired to perform the inspection wrote, "No corrosion of significant airworthy
The pilot's failure to maintain airplane control after he shut down the right engine in flight due a loss of oil pressure. Contributing to the accident was the pilot's decision to reposition the unairworthy airplane during twilight after extensive maintenance had been done to the right engine along with a known mechanical deficiency with the landing gear. Contributing to the accident was the mechanic's improper assembly and installation of the right engine's oil filter adapter, which resulted in a loss of oil to that engine.
Source: NTSB Aviation Accident Database
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