Aviation Accident Summaries

Aviation Accident Summary ERA13LA121

Yonkers, NY, USA

Aircraft #1

N1967E

PIPER PA-32-260

Analysis

The pilot was performing a personal sightseeing flight over the Hudson River at 1,200 feet above mean sea level. She reported the airplane contained 74 gallons of fuel at takeoff. While abeam a tower, the engine began to partially lose power. The pilot initiated the emergency procedures in the checklist and applied carburetor heat. Engine performance worsened and the carburetor heat was left on for about 15 seconds. She then turned off the carburetor heat and engine performance improved. After about 20 seconds, the engine began to lose power again. Unable to maintain altitude, she made a mayday call and performed a forced landing on the river. The engine and airframe were inspected after the airplane was recovered from the river. The engine ingested a significant amount of mud and debris and many engine components were corroded. No evidence of preaccident mechanical malfunction or failure was found with the engine, ignition system, or carburetor that would have precluded normal operation. Damage from prolonged water submersion prevented a test run of the engine. The airplane was not being operated in weather conditions conducive to carburetor icing.

Factual Information

On January 27, 2013, about 1730 eastern standard time, a Piper PA-32-260, N1967E, was substantially damaged following a partial loss of engine power and forced landing near Yonkers, New York. The commercial pilot and one passenger were not injured. The airplane was operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed and a visual flight rules flight plan was filed. The local flight originated at Old Bridge Airport (3N6), Old Bridge, New Jersey, about 1630. The pilot reported that she was conducting a personal sightseeing flight over the Hudson River at 1,200 feet mean sea level (msl). She reported the airplane contained 74 gallons of fuel at takeoff. As the aircraft was abeam the Alpine Tower, near Alpine, New Jersey, the engine started to “stutter.” She initiated the emergency procedures in the checklist and applied carburetor heat. Engine performance worsened and the carburetor heat was left on for about 15 seconds. She then turned off the carburetor heat and engine performance improved. She climbed the airplane to 1,200 feet, and after about 20 seconds, the engine began to stutter again. Unable to maintain altitude, she made a mayday call and prepared for a forced landing on the river. The airplane touched down smoothly on the surface of the water. The pilot and passenger exited the airplane and were rescued by first responders. The wreckage was recovered from the river bottom on February 7, 2013. The upper portion of the rudder and the nose landing gear were bent. The wreckage was recovered to a storage facility at Clayton, Delaware, where a detailed examination of the airframe and engine was performed. The fuel selector handle was in the “left main” tank position. The magneto switch was in the “both” position. All engine controls were in the “full forward” positions. The carburetor heat was found in the “cold” position and functioned normally when tested. Engine compression and suction were observed on all cylinders when the engine was rotated manually. The top of the engine was covered with mud. All of the ignition leads were removed and tested; the leads to the numbers 2 and 4 top spark plugs produced a spark when the crankshaft was rotated manually. No other leads would produce a spark. The top spark plugs were removed for inspection; the leads were covered with deposits and corrosion. The carburetor fuel inlet screen was removed and inspected; it contained a sand-like substance on the surface. The carburetor venturi was intact; however, it was lightly coated with mud and debris. A review of the Federal Aviation Administration (FAA) Special Airworthiness Information Bulletin, CE-09-35, dated June 30, 2009, revealed that the temperature and dew point at the nearest weather reporting station were not conducive to carburetor icing.

Probable Cause and Findings

A partial loss of engine power for reasons that could not be determined because examination of the engine and associated components did not reveal any mechanical malfunction or failure that would have precluded normal operation.

 

Source: NTSB Aviation Accident Database

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