Aviation Accident Summaries

Aviation Accident Summary WPR14LA112

Stanwood, WA, USA

Aircraft #1

N669DT

WEINZIERL SEAREY

Analysis

The noncertificated pilot reported that, following an uneventful local sightseeing flight, he conducted a low pass over a lake with glassy water conditions; he did not intend to land. The pilot thought the airplane was about 3 or 4 feet above the water when it suddenly skimmed the water's surface. The pilot pulled up, but the airplane subsequently nosed down into the water, and it became partially submerged. It is likely that the glassy water conditions adversely affected the pilot's depth perception, which led to his subsequent failure to judge the height above the water and resulted in the inadvertent touchdown. The pilot reported no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

Factual Information

On January 26, 2014, about 1615 Pacific standard time, an experimental amateur built light sport Weinzierl Searey amphibious airplane, N669DT, was substantially damaged during an inadvertent water landing near Stanwood, Washington. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91. The non-certified pilot and his passenger were not injured. Visual meteorological conditions prevailed and no flight plan was filed for the local personal flight which originated from Arlington, Washington about 1500. In a written statement and telephone conversation, the pilot reported to the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) that following a local sightseeing flight, he intended on conducting a low pass over Lake Goodwin prior to returning to Arlington. The pilot verified the landing gear was in the retracted position and that glassy water conditions were present before he performed a low pass with no intent to perform a landing. The pilot thought that he was about 3 to 4 feet above the water surface when the airplane suddenly skimmed the water surface for about 3 seconds. The pilot pulled up and the nose immediately went into the water. The pilot stated that water immediately began flowing into the cockpit area. The pilot added that the airplane was partially submerged about 3 to 5 seconds later. The NTSB IIC reviewed postaccident photos taken by a private individual about an hour after the accident occurred. The photos revealed that a majority of the bottom side of the hull was separated. The pilot reported no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.

Probable Cause and Findings

The noncertificated pilot’s failure to maintain clearance from water while maneuvering at a low altitude over glassy water conditions, which adversely affected his depth perception.

 

Source: NTSB Aviation Accident Database

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