Aviation Accident Summaries

Aviation Accident Summary ANC14IA028

South Naknek, AK, USA

Aircraft #1

N30541

PIPER PA 28-181

Analysis

The pilot reported that he was taxiing the airplane for departure when he and his passengers smelled smoke in the cabin. He shut the engine down, and he and the passengers then evacuated the airplane. After escorting the passengers to a safe location, he saw smoke coming from the engine cowling area and attempted to put out any fire with a fire extinguisher; however, his attempt to put out the fire was unsuccessful, and the fire continued to burn a majority of the fuselage. Due to extensive fire damage, the initiation source of the fire could not be determined.

Factual Information

On May 14, 2014, about 1400 Alaska daylight time, a Piper PA 28-181 airplane, N30541, was involved in a ground fire at the South Naknek Airport, South Naknek, Alaska. The commercial pilot and two passengers had evacuated the airplane prior to the fire, and were not injured. The airplane was being operated by King Air, Inc., Naknek, Alaska, as a visual flight rules (VFR) non-scheduled commuter flight under the provisions of 14 Code of Federal Regulations Part 135 when the incident occurred. Day, visual meteorological conditions prevailed, and a company flight plan was filed for the two mile flight to Naknek. In a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), the pilot stated that he was taxiing out for departure when he smelled smoke in the cabin. He verified with a passenger that indeed there was a smoke smell in the cabin, and then shut the airplane's engine down, and evacuated the airplane. After evacuating the airplane and escorting the passengers to a safe location, he saw smoke coming from the engine cowling area, and attempted to put out any fire with the airplane's fire extinguisher. His attempt to put out the fire was unsuccessful, and the fire continued to burn a majority of the airplane's fuselage. The airplane was equipped with a Lycoming O-360-A4M carburated, reciprocating engine. The engine was examined on scene by a Federal Aviation Administration safety inspector from the Anchorage Flight Standards District Office. Due to the extent of the fire damage, the inspector was unable to determine the initiation point of the fire. One of the recovered fuel fittings was sent to the NTSB Materials Laboratory for examination, and the examination revealed that the fracture surfaces were consistent with an overstress fracture while the fitting was at elevated temperatures. No indications of preexisting cracking were noted.

Probable Cause and Findings

A fire in the airplane’s engine compartment that initiated for reasons that could not be determined due to extensive fire damage.

 

Source: NTSB Aviation Accident Database

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