Aviation Accident Summaries

Aviation Accident Summary WPR14LA207

Arvin, CA, USA

Aircraft #1

N97038

CESSNA 182

Analysis

The commercial pilot reported that, while in cruise flight, he noticed that the engine oil pressure had dropped. He declared an emergency and was initially given a heading to the closest airport. About 2-3 minutes later, he heard rattling noises from the engine, then the cabin filled with black smoke. He identified an open field and maneuvered for a forced landing. The airplane hit a berm and bounced, hitting several more berms, until it came to rest inverted. On-scene photographs showed that the belly of the airplane was coated with engine oil aft of the engine firewall. An engine examination identified that the air-oil separator return line was not connected to the return port located on a cylinder rocker cover. Maintenance records showed that the pilot had performed an oil change 4.3 hours before the accident. Since the oil filter is located behind the air-oil separator return line, it is likely that the pilot removed the air-oil separator return line to access the oil filter and failed to reconnect the line after replacing the filter. While in flight, oil slowly drained out of the air-oil separator return line and open return port, coating the belly of the airplane, until the engine experienced catastrophic failure due to oil starvation.

Factual Information

On May 24, 2014, at 1211 Pacific daylight time, a Cessna 182Q, N97038, experienced a total loss of engine power and force landed in a field one mile south of Arvin, California. During the off airport landing the airplane nosed over, substantially damaging the tail and left lift strut. The airplane was registered to, and operated by, the commercial pilot under the provisions of 14 Code of Federal Regulations, Part 91, as a personal flight. Both the pilot and his single passenger received minor injuries. Visual meteorological conditions prevailed during the flight, and a visual flight plan was not filed. The flight originated at Corona Municipal Airport, Corona, California.The pilot stated that an hour into the flight, while over the Tehachapi Mountains, he noticed that the engine oil pressure had dropped, but the oil temperature and cylinder temperatures were normal. He declared an emergency to Bakersfield Approach and was initially given vectors to Bakersfield Municipal Airport. About 2-3 minutes later he started hearing rattling noises coming from the engine and then the cockpit filled with black smoke. He identified an open field on his left and maneuvered to make that field but didn't realize it had crop furrows. The airplane hit the first berm hard, bounced 3-4 times hitting berms along the way, then the nose wheel hit a berm and flipped the airplane over onto its back. On scene photos showed that the belly of the airplane was coated with engine oil aft of the engine fire wall. An examination of the airplane and engine by the NTSB Investigator-in-Charge (IIC) and a technical representative from Continental Motors Incorporated was performed on September 30, 2014. The engine time indicated on the tachometer was 2,861.6 (hours). Investigators found the air-oil separator return line disconnected from the oil return port located on the rocker cover of the engine's number 1 cylinder. Oil staining was evident on the lower engine cowling below the number 1 cylinder. It was noted that the engine oil filter was located behind the air-oil separator return line. The left engine case half, upper section above the No 4 cylinder, exhibited a 6 x 4 inch hole just aft of the oil filler neck. The cylinders were removed and the case was separated into its halves. The crankshaft main bearings exhibited normal wear with no heat discoloration. The number 3 crankshaft throw bearing was shiny & polished showing very little heat discoloration. The number 4 crankshaft throw was dark black with a few gouges and exhibited extreme heat distress. The number 5 crankshaft throw was black and exhibited extreme heat distress. The number 6 connecting rod attached to the crankshaft throw was discolored dark gray, consistent with heat distress. The internal section of the engine case in line with the number 3 & 4 crankshaft throws exhibited internal repeated impact marks, metal removal, and damage to the oil galleries on both sides of the engine case. Examination of the engine logbook revealed that the most recent annual inspection was performed on April 10, 2013, 2,828.2 hours total time, and 309.5 hours since major overhaul (SMOH). The last entry in the logbook was dated April 18, 2014, where the pilot/owner had performed an oil change, 2,857.3 hours total time

Probable Cause and Findings

The pilot’s failure to reconnect the air-oil separator return line after completing an oil change, which resulted in a total loss of engine power due to oil starvation.

 

Source: NTSB Aviation Accident Database

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