Aviation Accident Summaries

Aviation Accident Summary GAA16CA232

Simsbury, CT, USA

Aircraft #1

N3506M

PIPER PA 12

Analysis

Same as Factual Information

Factual Information

The pilot of the tailwheel equipped airplane reported that his approach to landing was faster than normal. He further reported that after the airplane bounced on touchdown he elected to abort the landing, but reported that it was too late because the airplane was at the end of the runway and impacted a fence, and nosed over. The airplane sustained substantial damage to the empennage. According to the pilot there were no preimpact mechanical failures or malfunctions with the airframe or engine that would have precluded normal operation. A review of recorded data from the automated weather observation station located about 4 miles to the east, revealed that, about 20 minutes after the accident the wind was 180 degrees true at 11 knots, visibility 10 statute miles, and sky clear. The airplane landed on runway 03. The Federal Aviation Administration has published the Advisory Circular (AC) 91-79A. This AC discusses the effect of a tailwind on landing distance and states in part: The effect of a tailwind on landing distance is significant and is a factor in determining the landing distance required. Given the airplane will land at a particular airspeed, independent of the wind, the principal effect of a tailwind on operational landing distance is the change in the ground speed at which the airplane touches down.

Probable Cause and Findings

The pilot's failure to attain the proper touchdown point and the airplane's subsequent impact with a fence during an attempted aborted landing.

 

Source: NTSB Aviation Accident Database

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