Aviation Accident Summaries

Aviation Accident Summary CEN16FA215

Jonesboro, AR, USA

Aircraft #1

N789MR

ROBINSON HELICOPTER COMPANY R44 II

Analysis

During the 2 to 3 hours before the accident, a witness saw the commercial pilot drinking from a cup that smelled like alcohol and noticed that he refilled the cup two or three times. He then heard the pilot say that he was going to put on an airshow. The helicopter lifted off at a 45° angle backward and upward, reach an altitude of about 125 ft, and then descend out of sight behind hangars. A postaccident examination revealed that the helicopter's tail contacted the ground behind the hangars resulting in separation of both tail rotor blades. The helicopter then rose above the hangars and began to spin. The helicopter descended again, impacted terrain, and burst into flames. The examination of the wreckage did not reveal evidence of any preimpact anomalies that would have precluded normal operation of the helicopter. Toxicology testing detected diphenhydramine, a sedating antihistamine, and elevated levels of ethanol in the pilot's blood and tissues. The pilot was most likely impaired by the combination of ingested alcohol and the use of diphenhydramine, both of which are central nervous system depressants. The impairing effects of the combination of these substances most likely contributed to his decision to fly after drinking alcohol as well as his inability to maintain control of the helicopter.

Factual Information

HISTORY OF FLIGHTOn June 12, 2016, about 1530 central daylight time, a Robinson Helicopter Company, R44 II, Raven, helicopter, N789MR, impacted terrain during takeoff from the Classic Airstrip (23AR), near Jonesboro, Arkansas. The commercial pilot, who was the sole occupant, was fatally injured. The helicopter was destroyed during the impact and subsequent ground fire. The helicopter was registered to Floyd Vuncannon Aviation Inc. and was operated by the pilot as a Title 14 Code of Federal Regulations Part 91 personal flight. Day visual meteorological conditions prevailed at the airport about the time of the accident, and the flight was not operated on a flight plan. The local flight was originating from 23AR at the time of the accident. A witness, who was visiting a friend at an airstrip located just west of 23AR, reported that before noon, he saw the accident pilot drinking from a red cup that smelled like alcohol. The pilot refilled the cup 2 or 3 times during the next 2 or 3 hours. During the day, he saw the pilot going between hangars. When the witness finished working on a task, he heard the pilot say that he was going to put on an airshow. The witness saw the accident pilot getting into his helicopter, which was located east of him on 23AR. The witness observed the helicopter lift off at a 45° angle backward and upward. The helicopter rose to about 125 ft and then descended out of sight behind hangars that were located between 23AR's runway and the west airstrip. The witness reported that he thought he "heard it hit" but the engine never shutdown. The helicopter began to rise upwards above the hangars and it began to spin around. It appeared that the tail rotor was not working and the skids were bent as if it had hit the ground. The helicopter continued to rise to about the same height as when it lifted off. The helicopter then descended again, impacted terrain, and burst into flames in the middle of the west airstrip. The witness stated that another witness nearby called 911 and they waited for first responders to arrive. PERSONNEL INFORMATIONThe 73-year-old pilot held a Federal Aviation Administration (FAA) commercial pilot certificate with airplane single-engine land, rotorcraft helicopter, rotorcraft gyroplane, and instrument airplane ratings. He also held a flight instructor certificate, expiring October 31, 2017, with airplane single engine, rotorcraft helicopter, and rotorcraft gyroplane ratings. He held a FAA second-class medical certificate issued on May 1, 2014, with the limitations that he "must wear corrective lenses and possess glasses for near and intermediate vision." At the time of that medical examination, he reported 6,000 hours total flight time and 110 hours in the 6 months before that examination. A review of excerpts from the pilot's logbook did not reveal an entry for a flight review. The logbook pages were not totaled, and the last entry was dated August 2, 2015. AIRCRAFT INFORMATIONN789MR, serial number 10561, was a Robinson R44 II, Raven, four-place, two-bladed, single main rotor, single-engine helicopter, with a spring and yield skid type landing gear. The primary structure of its fuselage was welded steel tubing and riveted aluminum sheet. The tailcone was a monocoque structure consisting of an aluminum skin. A Lycoming IO-540- AE1A5, serial number L-29728-48A, engine rated at 260 horsepower, powered the helicopter. However, according to the helicopter's type certificate, the engine had a 5-minute takeoff rating of 245 horsepower and a maximum continuous rating of 205 horsepower. A review of helicopter logbook excerpts that were provided by a FAA inspector, showed that the helicopter's last annual inspection was completed on July 2, 2015. At the time of that inspection, the helicopter had accumulated a total time of 1,242.1 hours. The helicopter manufacturer issued, R44 Service Bulletin (SB)-78B, on December 20, 2010, and issued a revised SB on September 28, 2012. The SB, in part, stated: TO: R44 and R44 II owners, operators, and maintenance personnel SUBJECT: Bladder Fuel Tank Retrofit ROTORCRAFT AFFECTED: R44 helicopters S/N 0001 thru 2064, and R44 II helicopters S/N 10001 thru 12890, unless previously accomplished. TIME OF COMPLIANCE: As soon as practical, but no later than 30 April 2013. BACKGROUND: This bulletin requires R44 helicopters with all-aluminum fuel tanks to be retrofitted with bladder-type tanks. In addition to a factory retrofit program, a field kit is now available. To improve the R44 fuel system's resistance to a post-accident fuel leak, this retrofit must be performed as soon as possible. The review of the helicopter logbook excerpts did not reveal an entry for the installation of the bladder fuel tanks as called for by the SB. METEOROLOGICAL INFORMATIONAt 1538, the recorded weather at the Jonesboro Municipal Airport, near Jonesboro, Arkansas, located about 5 miles west of 23AR, included wind 090° at 4 knots, visibility 10 statute miles, present weather thunderstorms in the vicinity, temperature 34° C, dew point 21° C, and altimeter 30.02 inches of mercury. AIRPORT INFORMATIONN789MR, serial number 10561, was a Robinson R44 II, Raven, four-place, two-bladed, single main rotor, single-engine helicopter, with a spring and yield skid type landing gear. The primary structure of its fuselage was welded steel tubing and riveted aluminum sheet. The tailcone was a monocoque structure consisting of an aluminum skin. A Lycoming IO-540- AE1A5, serial number L-29728-48A, engine rated at 260 horsepower, powered the helicopter. However, according to the helicopter's type certificate, the engine had a 5-minute takeoff rating of 245 horsepower and a maximum continuous rating of 205 horsepower. A review of helicopter logbook excerpts that were provided by a FAA inspector, showed that the helicopter's last annual inspection was completed on July 2, 2015. At the time of that inspection, the helicopter had accumulated a total time of 1,242.1 hours. The helicopter manufacturer issued, R44 Service Bulletin (SB)-78B, on December 20, 2010, and issued a revised SB on September 28, 2012. The SB, in part, stated: TO: R44 and R44 II owners, operators, and maintenance personnel SUBJECT: Bladder Fuel Tank Retrofit ROTORCRAFT AFFECTED: R44 helicopters S/N 0001 thru 2064, and R44 II helicopters S/N 10001 thru 12890, unless previously accomplished. TIME OF COMPLIANCE: As soon as practical, but no later than 30 April 2013. BACKGROUND: This bulletin requires R44 helicopters with all-aluminum fuel tanks to be retrofitted with bladder-type tanks. In addition to a factory retrofit program, a field kit is now available. To improve the R44 fuel system's resistance to a post-accident fuel leak, this retrofit must be performed as soon as possible. The review of the helicopter logbook excerpts did not reveal an entry for the installation of the bladder fuel tanks as called for by the SB. WRECKAGE AND IMPACT INFORMATIONThe main helicopter wreckage was located about 1,800 ft on a magnetic heading of 35° from the intersection of Highway 18 and Barnhill Road. The turf, in a circular shaped area around the helicopter was found charred. Portions or the helicopter wreckage were discolored, deformed, and consumed by fire consistent with a ground fire. The helicopter's resting heading was about 270° magnetic. The tailcone was folded to the left and separated near its forward end. Most of the aluminum and fiberglass components of the fuselage were discolored, deformed, and consumed by fire. The separated aft section of the tailcone was located about 20 ft south of the airframe. The tail rotor gearbox remained attached to the aft bulkhead of the separated section of the tailcone. The empennage separated from the aft bulkhead and was located about 40 ft south of the airframe. The main rotor gearbox and main rotor were separated from the airframe and found about 3 ft north of the airframe. Ground scars north of the airframe were consistent with main rotor blade strikes. Main rotor blade tip pieces were recovered in and near the ground scars and yellow paint that matched the paint on the main rotor blade tips was transferred to the dirt inside the scars. Both tail rotor blades were separated near their roots and were found east of the airframe on the other side of the hangar located between 23R and the west airstrip. A series of ground scars consistent with the shape, size, and spacing of tail rotor blade strikes were located east of the location that the tail rotor blades were found. An on-scene examination of the wreckage revealed that all flight control rod ends remained attached to their attachment points. Sections of push pull tubes were not continuous, separated from their original location, and/or consumed by fire. All flight control discontinuities exhibited either thermal damage or separations consistent with overload. No preimpact anomalies were detected in the flight control system. The fuel mixture control knob was found in the full rich position. The mixture control wire was found disconnected near its fuel mixture arm on the engine fuel control servo unit. The throttle linkage sustained thermal damage and its position could not be determined. The governor switch sustained thermal damage and its position could not be determined. The right skid tube was located under the main wreckage and it sustained thermal damage. The four struts that attached the left and right skid tubes were separated from the airframe and were thermally damaged. The aft cross tube appeared to be thermally deformed. A portion of the front cross tube was consumed by fire and the remaining end was not bent near its elbow. Observed damage to the cabin structure included deformation, discoloration, and consumption by fire. The removable cyclic and collective were recovered from under seat debris, and the removable pedals were installed. The pedals were found in a neutral position. The vertical tube of the cyclic control was bent aft. The cyclic grip was consumed by fire. The aft left and right doors were found in the main wreckage and they sustained thermal damage. The two front doors were not identified or found in the wreckage. The upper and lower frames were bent and had some separations in their tubes. The surface of the separations exhibited angular and jagged features consistent with overload. The lower edge of the vertical firewall was deformed. The tailcone was bent to the left and thermally damaged at its forward end. The separated aft section of the tailcone exhibited deformation damage consistent with several tail rotor blade strikes. The empennage was separated from the aft bulkhead. The surface of the separation was rough and jagged. The lower vertical stabilizer was bent to the right as viewed from its aft looking forward. A segment of the tail rotor guard that included the guard's curved section was separated below its forward mount and forward of its aft mount. The surfaces of the guard's separations were angular and jagged. The aft section of the tail rotor guard remained attached to its mount and the tip of the tail rotor guard exhibited witness marks consistent with scuffing on its lower left surface. The tailskid had some witness marks on its lowest bottom surface consistent with scuffing. Sections of the V-belts were consumed by fire with charred sections remaining in the grooves of the upper sheave and on the ground below the lower sheave. The alignment strut's outer rod end for the upper sheave exhibited a separation consistent with overload. No scoring was visible on the sheave face. Scoring was visible on the rod end jam nut adjacent to the aft sheave face. The overrunning clutch operated properly. The actuator was extended about 1 inch. The main rotor gearbox was separated at the upper housing. The main rotor driveshaft was bent about 15° at the swashplate. The mast tube was bent and exhibited thermal discoloration and damage. Both elastomeric teeter stops were consumed by fire and their brackets were bent across the center. One droop stop tusk was bent downward and the spindle was found cracked with and an angular and jagged separation surface. The other spindle coning bolthole was deformed. Both main rotor blades exhibited thermal damage and deformation consistent with impact damage. The lower frame tube adjacent to the intermediate flex coupling exhibited rotational scoring. The tail rotor driveshaft was bent near its forward end and was disconnected just aft of the bend. The tail rotor drive shaft damper bearing bracket was separated from the bulkhead. The damper bearing exhibited thermal damage and would not rotate. The tail rotor gearbox rotated with no anomalies. Oil was visible in its sight gage. The blades were separated near their roots. The surface of the tail rotor blades' separations exhibited angular and jagged features consistent with overload. Both blades were bent to the right and they exhibited leading edge damage at their tips. One blade exhibited deformation damage that was consistent with contact with rivet locations on the tailcone. Witness marks running chordwise near the blade tips were present on both blades, which appeared to be consistent with terrain contact. Observed damage to the cooling fan included discoloration and it was deformed around its forward edge. The cooling scroll was consumed by fire. The alternator and its cooling fan exhibited thermal damage. The engine was found lying upright and it remained attached to its tubular engine mounts. The exterior surfaces of the engine were discolored consistent with exposure to a post-impact fire. Sections of the oil sump were consumed in the fire. The fuel servo was found separated and partially thermally consumed. The remaining rear mounted accessories exhibited features consistent with fire damaged. The engine was partially disassembled. The engine's crankshaft was rotated by turning the cooling fan, and continuity of the crankshaft to the rear gears and to the valve train were confirmed. Thumb compression and suction were observed from all six cylinders as the engine was rotated. The interiors of the cylinders were examined using a lighted borescope and no anomalies were noted. The two-piece fuel injector nozzles were disassembled and found to be unobstructed. Disassembly of both magnetos revealed that their internal components sustained thermal damage. The removed sparkplug electrodes exhibited light brown coloration and worn out normal condition when compared to the Champion Check-A-Plug chart. MEDICAL AND PATHOLOGICAL INFORMATIONThe Arkansas State Crime Lab Medical Examiner's Office conducted an autopsy on the pilot and took toxicological samples. The autopsy indicated that the pilot's cause of death was multiple blunt force injuries and the manner of death was an accident. No significant natural disease was identified during the autopsy. The FAA Bioaeronautical Sciences Research Laboratory performed toxicological testing on the samples taken during the autopsy. The toxicology report indicated that the samples sustained putrefaction and listed the following findings: 418 (mg/dL, mg/hg) Ethanol detected in Blood 336 (mg/dL, mg/hg) Ethanol detected in Heart 309 (mg/dL, mg/hg) Ethanol detected in Lung 182 (mg/dL, mg/hg) Ethanol detected in Kidney 152 (mg/dL, mg/hg) Ethanol detected in Urine ... Diphenhydramine detected in Urine 0.049 (ug/ml, ug/g) Diphenhydramine detected in Blood Pioglitazone detected in Urine Valsartan detected in Urine Valsartan detected in Blood Ethanol is the intoxicant commonly found in beer, wine, and liquor. It acts as a central nervous system (CNS) depressant. After ingestion, at low doses, it impairs judgment, psychomotor functioning, and vigilance; at higher doses it can cause coma and death. The effects of ethanol on aviators are generally well understood; it significantly impairs pilots' performance, even at very low levels. Federal Aviation Regulations prohibit any person from acting or attempting to act as a crewmember of a civil aircraft while having 0.040 gm/dl (40 mg/dl) or more ethanol in the blood. Ethanol may also be produced in the body after death by microbial activity. Diphenhydramine is a sedating antihistamine used to tre

Probable Cause and Findings

The pilot's failure to maintain helicopter control during takeoff. Contributing to the accident was the pilot's impairment due to his combined use of alcohol and diphenhydramine, which led to his improper decision to fly after drinking alcohol and degraded his ability to maintain control of the helicopter.

 

Source: NTSB Aviation Accident Database

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