Windsor Twp, PA, USA
N3846T
LAZEAR JOHN T ZENAIR STOL CH 701
The pilot of the experimental, amateur-built airplane reported that he attempted to take off on a grass portion of his property that extended about 1,000 ft before reaching power lines. During takeoff on an approximate 130° heading, he noticed the airplane was not climbing fast enough to clear the power lines. He pulled up "hard" to clear the power lines but stalled the airplane. The left wing dipped down, and the airplane impacted the ground. The right wing separated from the fuselage, and the empennage was crushed behind the wings. Both main landing gear separated from the fuselage, and the nose landing gear folded back under the engine compartment. The pilot reported that there were no preimpact mechanical malfunctions or anomalies with the airplane that would have precluded normal operation. He added that he thought the wind was swirling and that the airplane may have encountered some wind shear. The recorded wind at an airport located about 13 miles west of the accident site, about the time of the accident, was from 320° at 4 knots.
The pilot of the experimental amateur-built airplane reported that he attempted to takeoff on a grass portion of his property, that extended about 1,000 ft prior to reaching powerlines. During takeoff on an approximate 130° heading, he noticed the airplane was not climbing fast enough to clear the powerlines. He pulled up "hard" to clear the powerlines but stalled the airplane. The left wing dipped down and the airplane impacted the ground. The right wing separated from the fuselage and the empennage was crushed behind the wings. Both main landing gear separated from the fuselage, and the nose gear folded back under the engine compartment. The pilot reported there were no preimpact mechanical malfunctions or anomalies that would have precluded normal operation of the airplane. He added that he thought the wind was swirling and may have encountered some windshear. The recorded wind at an airport located about 13 miles west of the accident site, about the time of the accident, was from 320° at 4 knots.
The pilot's improper pretakeoff planning, his failure to maintain adequate airspeed, and his exceedance of the airplane's critical angle of attack during a short-field takeoff with a tailwind, which resulted in an aerodynamic stall.
Source: NTSB Aviation Accident Database
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