Blythe, CA, USA
N418CP
CIRRUS DESIGN CORP SR22
The flight instructor reported that he and the pilot receiving instruction were conducting an instructional, cross-country flight. About 1.3 hours into the flight, the oil pressure started to decrease, and the pilots decided to divert to a nearby airport. The oil pressure continued to decrease, and the engine subsequently lost all power. The airplane was unable to reach the runway, so the pilots chose to activate the parachute system. Upon ground impact, the parachute dragged the airplane for about 20 ft. The pilots then egressed the airplane, and the parachute then dragged it another 200 ft. The nose landing gear and left main landing gear collapsed, and the fuselage and engine firewall sustained substantial damage. During postaccident examination of the airframe, an oil streak was observed covering the airplane’s belly. During engine examination, a b-nut fitting that attached the oil supply line to the turbocharger inlet check valve was found loose. A significant amount of fresh oil was observed in the area around the b-nut fitting and on the engine’s right side near the turbocharger next to the b-nut. The cowling bottom’s right side exhibited significantly more oil staining than the bottom’s left side. The b-nut and its threads were not damaged. A small hole was found on the top of the engine crankcase, consistent with an internal engine failure. A review of the airplane’s maintenance records revealed that an annual inspection was completed earlier on the day of the accident flight and that actions were taken to comply with a turbocharger manufacturer's safety bulletin that recommended that the turbocharger oil supply inlet screen be inspected and cleaned on a regular basis. To inspect and clean the inlet screen, the oil line to the turbocharger bearing housing inlet and cap has to be removed, followed by the removal of the valve assembly from the turbocharger oil inlet fitting. The valve assembly must then be reassembled, during which the check valve should be torqued to 85-inch lbs. The valve assembly should then be reinstalled on the turbo oil adapter and torqued to 85-inch lbs. It is likely that, during the maintenance, maintenance personnel failed to properly torque the b-nut fitting that attached to the turbocharger inlet check valve oil line supply line to the turbocharger inlet check valve, which resulted in oil starvation and a subsequent engine failure.
On October 3, 2017, about 1521 Pacific daylight time, a Cirrus Design Corp SR22 airplane, N418CP, was substantially damaged when it was involved in an accident near Blythe, California. The flight instructor and pilot sustained minor injuries. The airplane was being operated as a Title 14 Code of Federal Regulations Part 91 instructional flight. According to the flight instructor, the purpose of the cross-country flight was to reposition the airplane for the new owner and provide advanced transition training to the other pilot onboard. He and the pilot receiving instruction met before the flight to review the airplane's logbooks and plan the flight. The fuel tanks were filled, and neither the instructor nor the pilot saw any oil residue on the airplane’s belly during the preflight inspection. According to flight data recorder data, after an uneventful takeoff about 1347:22, the airplane climbed and then leveled off at a cruise altitude of about 11,500 ft mean sea level about 1359:38. About 1505:00, the oil pressure started to decrease. About 1.5 minutes later, the oil pressure had decreased to less than 30 pounds per square inch (psi). The instructor reported that, subsequently, they decided to divert to Blythe Airport (BLH), Blythe, California. While inbound to BLH, the oil pressure continued to decrease to less than 5 psi. Shortly thereafter, the engine lost all power. The airplane was unable to reach the runway, so the pilots chose to activate the airplane's parachute system when the airplane was about 2,000 ft above ground level. The parachute successfully deployed, and upon ground impact, the parachute dragged the airplane about 20 ft. The pilots then egressed the airplane, and the parachute dragged it another 200 ft, during which the nose landing gear and left main landing gear collapsed. A review of maintenance records revealed that an annual inspection was completed earlier on the day of the accident flight and that actions were taken to comply with the turbocharger manufacturer’s Safety Bulletin (SB) TAT SB11-04, which instructed owners “to have the turbocharger oil supply inlet screen inspected and cleaned on a regular basis to ensure that the turbo system continues to function properly.” To inspect and clean the inlet screen, the oil line to the turbocharger bearing housing inlet and cap has to be removed, followed by the removal of the valve assembly from the turbocharger oil inlet fitting. The valve assembly then needs to be reassembled, during which a thread sealant should be applied on the external threads of the check valve before screwing the check valve adapter onto it, and the adapter should be torqued to 85 inch-lbs. The valve assembly should then be reinstalled on the turbo oil adapter with a thread sealant applied and torqued to 85 inch-lbs. The SB instructs maintenance personnel to conduct a postmaintenance ground run of the engine to check for any oil leaks after shutdown. The maintenance records indicated that maintenance personnel conducted a ground run, and they did not note any oil leaks. Postaccident examination of the airplane revealed that the fuselage and engine firewall were substantially damaged. Further, the b-nut fitting that attached the oil supply line to the turbocharger inlet check valve was found loose, and it was able to be rotated by hand. A significant amount of fresh oil was observed in the area around the b-nut fitting and on the engine’s right side near the turbocharger next to the b-nut. The cowling bottom’s right side exhibited significantly more oil staining than the bottom’s left side. The b-nut and its threads were not damaged. No additional anomalies associated with the turbocharger were found. The engine remained attached to all its mounts, and no external cylinder damage was observed. All engine accessories remained attached to their mounts. A small hole was found on the top of the engine crankcase, consistent with an internal engine failure. No anomalies were noted with the ignition components, the exhaust system, or the induction system. The left and right magnetos remained attached and were intact. No evidence of oil leaks was observed around the magneto mounting flange. All the spark plugs remained installed and were intact. The bottom spark plugs exhibited normal wear and operating signatures Boroscopic examination of the engine’s internal surfaces revealed that the Nos. 3 and 4 connecting rods had separated from the crankshaft. The journal for one of the separated connecting rods was visible, and it exhibited thermal damage consistent with lubrication distress. The No. 4 cylinder exhibited normal operating and combustion signatures. The No. 3 cylinder was only partially visible because of the piston position, and the visible portion exhibited normal operating and combustion signatures. The fuel pump remained attached and was intact. All the fuel lines remained secured to the fuel pump, and no fuel leaks were observed. No oil leaks were observed around the area of the fuel pump mounting flange. The throttle and metering assembly remained attached and was intact, and no anomalies were noted. The oil pump, filter, and oil sump remained attached and were intact, and no evidence of oil leaks were observed near these components. The quick oil drain valve remained secured and was in the “closed” position. The oil gauge indicated that the oil sump contained about 2 quarts of oil. A significant amount of metallic material consistent with bearing, piston, and crankcase material was found in the oil sump. The bearing pieces exhibited thermal damage, consistent with lubrication distress. The oil pick-up tube was partially visible, and no anomalies were noted. During examination of the oil filter pleats, a small amount of residual oil and several pieces of metallic material were observed. The oil cooler remained attached and was intact, and no evidence of oil leaks was found near it or its attaching lines. All the oil lines were secured, and no evidence of oil leaks were found in the lines or surrounding area. The propeller flange remained attached to the crankshaft, and no cracks were found in the crankshaft’s exterior. The crankshaft was able to be rotated by hand using the propeller with noticeable resistance, and rotational continuity was established throughout the engine and valve train.
Maintenance personnel's failure to properly torque an oil supply line fitting, which resulted in oil starvation, a subsequent engine failure, and an off-airport landing.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports