Aviation Accident Summaries

Aviation Accident Summary GAA18CA149

Ferris, TX, USA

Aircraft #1

N77MM

BEECH B

Analysis

The pilot in the multi-engine, retractable landing gear airplane reported that, during an instrument flight rules cross-country flight, about 5,000 ft above mean sea level, the left engine surged several times and he performed an emergency engine shutdown. Shortly afterward, the right engine lost power. During the emergency descent, the airplane struck treetops, and landed hard in a field with the landing gear retracted. The airplane sustained substantial damage to both wings, the engine mounts, and the lower fuselage. The pilot reported that he had requested 200 gallons of fuel from his home airport fixed base operator, but they did not fuel the airplane. The pilot did not check the fuel quantity during his preflight inspection. According to the Federal Aviation Administration Airplane Flying Handbook, Chapter 2, page 2-7, pilots must always positively confirm the fuel quantity by visually inspecting the fuel level in each tank. The pilot reported that there were no mechanical malfunctions or failures with the airplane that would have precluded normal operation.

Factual Information

The pilot in the multi-engine, retractable landing gear-equipped airplane reported that during an instrument flight rules cross-country flight, about 5,000ft MSL, the left engine surged several times and he performed an emergency engine shutdown. Shortly afterward, the right engine lost power. During the emergency descent, the airplane struck tree tops, and landed hard in a field with the landing gear retracted. The airplane sustained substantial damage to both wings, the engine mounts and the lower fuselage. The pilot reported that he had requested 200 gallons of fuel from his home airport FBO, but they did not fuel the airplane. The pilot did not check the fuel quantity during his preflight inspection. According to the Federal Aviation Administration Airplane Flying Handbook, Chapter 2, page 2-7, pilot's must always positively confirm the fuel quantity by visually inspecting the level of each tank. The PIC reported that there were no mechanical malfunctions or failures with the airplane that would have precluded normal operation.

Probable Cause and Findings

The pilot’s improper preflight inspection of the fuel level, which resulted in a loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot’s failure to lower the landing gear before the emergency landing.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports