Aviation Accident Summaries

Aviation Accident Summary WPR19LA060

San Diego, CA, USA

Aircraft #1

N4161X

Piper PA46

Analysis

The pilot reported that the airplane began to pull to the left shortly after touchdown. He applied corrective control inputs, but the airplane continued to veer left and departed the runway, and the main landing gear collapsed. Examination did not reveal any anomalies with the steering system that would have precluded normal operation, and all appropriate service bulletins had been complied with. The nose gear actuator had detached at an area on the airframe that was prone to fatigue failure; however, examination of the actuator assembly revealed that it had detached during an overload event, likely from the impact as the airplane departed the runway.

Factual Information

On December 30, 2018, at 1553 Pacific standard time a Piper PA46-350P, N4161X, was substantially damaged when it was involved in an accident near San Diego, California. The private pilot and three passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot stated that the landing approach and flare to runway 28R were normal and the touchdown was smooth. Shortly after the nose landing gear made contact with the ground, the airplane started to pull to the left. He applied corrective control inputs, but the airplane continued to turn left. The airplane then departed the runway surface, and the landing gear collapsed. Both wings and the aft cabin structure sustained substantial damage during the accident sequence, and all occupants were able to egress from the aft cabin door unaided. Due to the US federal government shutdown of 2018–2019, the NTSB was unable to respond to this accident, gather perishable evidence (such as tire pressures, or the airplane’s immediate postaccident state), or oversee the airplane’s removal to a secure facility. An examination of the airplane was ultimately performed by the NTSB on February 19, 2019. A complete examination report is contained in the public docket. Photographic evidence provided by the manager of a local fixed base operator, who recovered the airplane, indicated that it came to rest about 1,300 ft beyond the displaced threshold of runway 28R, and 50 ft left of the runway edge. Runway 28R was 4,598 ft long, and 150 ft wide. The main landing gear had collapsed, and three black tire transfer marks were present in a sweeping arc from the runway centerline through to the area where the airplane entered the adjacent infield. Examination of the airplane revealed that both the left and right landing gear actuators were in the extended position. The left actuator had detached from its mounting points at both the wing spar and the landing gear trunnion. The right actuator remained attached to the trunnion; its piston was bent, and the upper section of the actuator had detached from the wing spar. All failure areas exhibited grainy surface features, and there was no evidence of corrosion or beach markings on any of the detached faces. The nose landing gear had partially retracted and rotated, with the wheel hanging just below the open gear doors. The oleo strut and trunnion assembly remained attached to the fuselage, the scissor link appeared undamaged, and the steering horn remained attached to the nosewheel. The down spring was intact, the tire was firm, and the left side of the tire lip exhibited scuffing and material removal when compared to the right edge, which was undamaged. The lower section of the landing gear actuator remained attached to the trunnion, and the upper section had broken free from its engine mount attach point and was impinging against the firewall. The actuator’s internal locking system appeared to have engaged, and the piston exhibited 7 1/8 inches of extension, consistent with full landing gear extension. Control continuity was established from the foot pedals aft to the rudder and from the foot pedals forward to the steering bellcrank, bungee, and steering arm; movement of the foot pedals resulted in appropriate movement of the steering arm. With the actuator removed, the nose landing gear trunnion fell forward, and the gear locked into place with the aid of the down spring. In this mode, the steering arm made contact with the steering horn and rollers, and no significant play was observed. Subsequent movement of the foot pedals resulted in appropriate steering movement of the nose wheel. The brake lines sustained damage, preventing an accurate assessment of the brake system; however, both wheels could be freely rotated, and both rotors were bright in appearance, with no evidence of thermal discoloration. A series of five Piper service bulletins (SB) relating to the steering system were applicable to the accident airplane. SB 1060 required the removal of a spring washer in the pin that attached the brake pedal to the master cylinder. It had been discovered that the spring washer could potentially restrict rudder medal movement, resulting in binding brakes, and inconsistent ground steering. Maintenance records indicated that the SB had been complied with in November 2001. SB 1075 called for the modification of the steering horn to prevent contact with the engine mount during ground tow. Maintenance records indicated that the SB had also been complied with in November 2001. SB 1256 Provided instructions for replacing the nut and reorienting the bolt used to connect the upper and lower torque links on the nose landing gear after it was discovered that, under certain conditions, use of tow straps may cause the loss of the nut cotter pin. Maintenance records indicated that the SB had been complied with in August 2013. SB 1103F called for a repetitive fluorescent penetrant inspection of the engine mount for fatigue cracks in the area of the nose landing gear actuator attach point. It was required to be performed at 100-hour intervals unless the airplane was upgraded with a strengthened engine mount. The airplane appeared to have the original engine mount, and maintenance records indicated that it was inspected in accordance with SB 1103F during the last annual inspection on January 26, 2018, 52.2 flight hours prior to the accident. SB 1193 recommended the replacement of the nose landing gear down spring due to its tendency to develop a permanent set over time. The SB stated that failure to replace the spring could result in the nose landing gear taking an excessively long time to extended. Maintenance records indicated that the spring was replaced at the last annual inspection. The actuator and the damaged upper engine mount components were removed for further examination at the NTSB Materials Laboratory to confirm compliance with SB 1103F. Examination revealed that the engine mount had fractured in the area specified by SB 1103F: at the right attachment foot for the actuator and at one of the support tubes on the left attachment foot. The nose landing gear actuator remained bolted to pieces of the left and right attachment feet. The fractures were examined using an optical stereomicroscope, and all fracture features had a uniform matte-gray appearance on slant angles, consistent with ductile overstress fracture. A complete examination report is contained in the public docket. At the time of the accident, the wind was from 210° at 8 knots.

Probable Cause and Findings

Loss of directional control during the landing roll for reasons that could not be determined based on the available information.

 

Source: NTSB Aviation Accident Database

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