Hollister, CA, USA
N28CU
North American T28
The pilot reported that, after takeoff and while the airplane was about 500 ft above ground level, he retracted the landing gear and that, shortly thereafter, the engine sputtered and lost power. He adjusted the fuel mixture, but it did not have any effect. He attempted to return to the airport, but after realizing that the airplane would not reach the runway, he decided to land in a dirt field near the airport with the landing gear retracted. He recalled that he had the airplane refueled about a week before the accident. The airplane sustained substantial damage to the fuselage. The Federal Aviation Administration inspector who examined the airplane reported that he only removed about 1 or 2 cups of fuel out of the fuel system. The airplane was equipped with only one fuel gauge, which had a single switch that had left, right, and center positions. In the left position, it showed empty; in the center position, which showed the total fuel onboard, it showed 900 lbs; and in the right position, it also showed 900 lbs. No fuel leaks were found, and there were no signs of fuel on the ground. The pilot reported as a safety recommendation to "always top off fuel."
The pilot reported that, after takeoff, about 500 ft above the ground he retracted the landing gear and shortly thereafter, the engine sputtered and lost power. He adjusted the fuel mixture, but it did not have any effect. He attempted to return to the airport but noticed he would not make the runway and decided to land in a dirt field near the airport with the landing gear retracted. He recalled having refueled the airplane about a week prior. The pilot further reported that as a safety recommendation to "Always top off fuel." The airplane sustained substantial damage to the fuselage. The Federal Aviation Administration inspector who examined the airplane reported that, upon sumping the center tank and both wing tanks, he was only able to obtain about a cup or two of fuel out of the system. He further checked the fuel gauge; there was only one gauge for the fuel with a single switch which has left, right, and center positions. In the left position, it showed empty, in the center position, which showed total fuel, it read 900 lbs. and on the right position, it also showed 900 lbs. He further added that the mechanic that assisted with the recovery, said there was no fuel leaks and there were no signs of fuel on the ground. He also stated that they did not remove any fuel from the aircraft.
The pilot's improper fuel planning, which resulted in fuel exhaustion and the subsequent total loss of engine power.
Source: NTSB Aviation Accident Database
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