Ankeny, IA, USA
N83032
Aeronca 7AC
The pilot reported that he attempted to hand prop the engine numerous times without success. He returned to the cockpit and turned the magneto switch to the "off" position and advanced the throttle to between 1/2 and 3/4 travel. He then exited the cockpit and turned the propeller backward five to six "blades" to clear the cylinders. The pilot again returned to the cockpit and turned the magneto switch back to the "on" position, but he did not retard the throttle back to idle. He attempted to hand prop the engine again, and it started. Due to the engine's throttle setting, the airplane moved forward over the wheel chocks and struck the pilot, which resulted in serious injuries, and then a hangar, which resulted in substantial damage to the firewall and fuselage.
The pilot attempted to hand-prop the airplane's engine without success. He turned off the magneto switch and advanced the throttle to between ½ to ¾ travel and then turned the propeller backwards 5-6 times to clear the cylinders. The pilot reported that he returned to the cockpit and turned the magneto switch back to the on position but did not put the throttle back to idle. He hand-propped the airplane a second time and the engine started. The engine's throttle setting allowed the airplane to move forward over the wheel chocks, and the airplane struck the pilot. A passenger was still in the airplane as it collided with a hangar, resulting in substantial damage to the airplane's firewall and fuselage. The pilot was seriously injured, and the passenger was not injured.
The pilot's improper starting procedure, which allowed the airplane to move forward over the wheel chocks and impact him and a hangar when he subsequently hand propped the engine.
Source: NTSB Aviation Accident Database
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