Little Falls, MN, USA
N7013W
M-SQUARED Sport 1000
The uncertificated pilot stated that he replaced the wing and control surface skins of the airplane and planned to perform a test flight. He said that shortly after adding power, the airplane "jumped up" 15 ft off the ground and drifted away from the runway centerline. The pilot applied corrective control inputs to return the airplane back to runway centerline and then applied full engine power to initiate a go-around. About 100 ft agl, the airplane banked hard to the left. The pilot applied right aileron control input but was unable to reduce the bank. The airplane descended and impacted the ground about 200 yards from the end of the runway. The pilot stated that there were no engine-related mechanical anomalies. The flight controls were subject to impact damage; however, the damage was consistent with failures associated with overload due to ground impact and not a failure in flight.
The uncertificated pilot's failure to maintain aircraft control during takeoff, which resulted in an impact with terrain.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports