Aviation Accident Summaries

Aviation Accident Summary ERA20LA273

Knoxville, TN, USA

Aircraft #1

N55GJ

Eurocopter EC130

Analysis

The helicopter pilot was returning to his property located adjacent to a river. As the helicopter descended toward the water at a 25° angle with low forward airspeed, the pilot applied power to arrest the descent. However, the helicopter continued to descend until it impacted the river short of the intended landing area. The pilot and two passengers survived the impact and a third passenger drowned. The investigation revealed no preimpact mechanical malfunctions or anomalies that would have prevented the normal operation of the helicopter. Recovered flight data indicated the engine was producing power at the time of impact. Weather reports and statements from the pilot and witnesses indicated that the helicopter descended steeply with little forward airspeed and a tailwind of about 5 knots, which is a flight profile conducive to vortex ring state. The pilot’s reported lack of collective authority when increasing power to arrest the helicopter’s descent is also consistent with the helicopter entering vortex ring state. A pilot's failure to monitor altitude, airspeed, and rate of descent during an approach can result in a flight profile conducive to vortex ring state.

Factual Information

HISTORY OF FLIGHTOn August 3, 2020, at 1941 eastern daylight time, an Airbus EC130-B4 helicopter, N55GJ, was substantially damaged when it was involved in an accident near Knoxville, Tennessee. One passenger was fatally injured, and the pilot and two additional passengers were not injured. The helicopter was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. After refueling the helicopter, the pilot and his passengers departed McGhee Tyson Airport (TYS), Knoxville, Tennessee, about 1826 for a flight in the local area. About 1940 the pilot made a right circling approach over the Tennessee River toward a landing site on his property near the river’s edge. He stated that he “was descending with low power and a 25° angle of descent, slowing to come to a hover at low speed over the water.” He further stated that he was planning to hover taxi to the landing site at a height about 75 feet above the water and that when he added power to arrest the descent, the helicopter “started to settle.” He stated he “pulled max power to stop the settling,” but it was as if the helicopter “didn't have any power” and it continued to descend until it impacted the river. A witness on the neighboring property reported that the helicopter “came from the south and kind of hovered over the water pretty low.” She stated that it hovered longer than usual before tilting toward the south and descending into the water. A passenger stated that when the helicopter descended toward the water in a level attitude, the left “skid hit and then rotor hit” and the helicopter was “torqued into the water on the left side.” The pilot and two of the passengers were able to egress the helicopter before it sank; however, one passenger was unable to egress and was subsequently recovered by first responders. A pilot who had previously flown with the accident pilot reported that he spoke to the accident pilot the morning after the accident. He stated that the accident pilot recalled he was making a steep approach and he “came in vertically with little-to-no airspeed,” estimating that his descent rate was greater than 300 feet per minute. AIRCRAFT INFORMATIONAccording to the helicopter’s flight manual, and the helicopter’s weight and balance chart, the helicopter’s gross weight at the time of the accident would have been about 4,440.2 lbs. The limitations section of the helicopter's flight manual indicated a maximum gross weight of 5,350 lbs. The longitudinal and lateral CG locations were within flight manual limits. AIRPORT INFORMATIONAccording to the helicopter’s flight manual, and the helicopter’s weight and balance chart, the helicopter’s gross weight at the time of the accident would have been about 4,440.2 lbs. The limitations section of the helicopter's flight manual indicated a maximum gross weight of 5,350 lbs. The longitudinal and lateral CG locations were within flight manual limits. WRECKAGE AND IMPACT INFORMATIONExamination of the accident site by a Federal Aviation Administration (FAA) inspector revealed that the helicopter came to rest on the bottom of the Tennessee River about 435 ft and 149° from the intended landing site on the pilot’s property. The helicopter’s fenestron was recovered floating nearby. The helicopter was recovered from the river mostly intact. Examination of the wreckage revealed a large hole in the left side windshield; the left door window broken out; damage to all rotor blades consistent with water impact; and two of the four suspension bars fractured midspan. The tailboom remained attached to the fuselage, and the fenestron separated from the tailboom just aft of the ring frame. Examination of the airframe and flight control system components revealed no evidence of a pre-impact failure or mechanical malfunction that would have precluded normal operation, and the pilot reported that there were no mechanical malfunctions or failures prior to the accident sequence. The helicopter was equipped with a vehicle and engine monitoring display and a digital engine control unit that stored records of failure messages associated with engine operations. The data revealed no failures or limit exceedances prior to impact and indicated the engine was running at the time of impact. All failure indications occurred around the time of impact. No preimpact anomalies were noted with the engine that would have precluded the normal production of power. ADDITIONAL INFORMATIONVortex Ring State According to the FAA's Helicopter Flying Handbook (FAA-H-8083-21B), vortex ring state, formerly referenced as settling-with-power, "describes an aerodynamic condition in which a helicopter may be in a vertical descent with 20 percent up to maximum power applied, and little or no climb performance: Situations that are conducive to a vortex ring state condition are attempting to hover out of ground effect (OGE) without maintaining precise altitude control, and approaches, especially steep approaches, with a tailwind component. The following combination of conditions is likely to cause settling in a vortex ring state in any helicopter: 1. A vertical or nearly vertical descent of at least 300 fpm. (Actual critical rate depends on the gross weight, rpm, density altitude, and other pertinent factors.) 2. The rotor disk must be using some of the available engine power (20–100 percent). 3. The horizontal velocity must be slower than effective translational lift. When recovering from a vortex ring state condition, the pilot tends first to try to stop the descent by increasing collective pitch. The traditional recovery is accomplished by increasing airspeed, and/or partially lowering collective to exit the vortex. In most helicopters, lateral cyclic thrust combined with an increase in power and lateral antitorque thrust will produce the quickest exit from the hazard.” According to the FAA's Helicopter Flying Handbook, hovering more than one main disc (rotor) diameter above the surface is considered hovering OGE. The accident helicopter rotor diameter was 35 ft 1 in.

Probable Cause and Findings

The pilot's entry into vortex ring state and his inability to arrest the helicopter's descent while maneuvering for landing.

 

Source: NTSB Aviation Accident Database

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