Aviation Accident Summaries

Aviation Accident Summary CEN20LA361

Crowley, LA, USA

Aircraft #1

N639RR

Cessna R182

Analysis

About 30 minutes into the aerial observation flight, the engine began "popping" and running rough. The pilot was unable to maintain sufficient engine RPMs and elected to return to the departure airport for a precautionary landing. Based on the airplane's location relative to the runway orientation, the pilot performed a downwind landing. During the approach, the airplane was "a little high and fast;" however, the pilot was committed to the landing due to the reduced engine performance. The airplane touched down, overran the end of the turf runway impacted a ditch and came to rest upright. Both wings and the fuselage sustained substantial damage. Postaccident examination of the engine revealed the No. 4 engine cylinder exhaust valve was stuck which resulted in a bent push rod and partial loss of engine power. Due to damage to the operator's facility and the airplane from hurricane activity, further examination of the engine was not conducted and the reason for the stuck valve was not determined.

Factual Information

On August 24, 2020, about 0935 central daylight time, a Cessna R182 airplane, N639RR, was substantially damaged when it was involved in an accident near Crowley, Louisiana. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 aerial observation flight. According to the pilot, the preflight engine run-up and takeoff were normal. About 30 minutes into the aerial observation flight, the engine began "popping" and running rough. The pilot was unable to maintain sufficient engine RPMs and elected to return to the departure airport for a precautionary landing. Based on the airplane's location relative to the runway orientation, the pilot performed a downwind landing. During the approach, the airplane was "a little high and fast;" however, the pilot was committed to the landing due to the reduced engine performance. The airplane touched down, overran the end of the turf runway, impacted a ditch and came to rest upright. The pilot reported the airplane sustained substantial damage to both wings and the fuselage. Postaccident examination of the engine by the operator revealed the No. 4 engine cylinder exhaust valve was stuck which resulted in a bent push rod and partial loss of engine power. Following the accident, hurricane activity damaged the operator's facility and the accident airplane, and further examination of the engine was unable to be conducted.

Probable Cause and Findings

The failure of the No. 4 cylinder exhaust valve that resulted in a partial loss of engine power. Based on available evidence, the reason for the failed valve was not determined.

 

Source: NTSB Aviation Accident Database

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