Aviation Accident Summaries

Aviation Accident Summary ERA20LA297

Pembroke Park, FL, USA

Aircraft #1

N900DT

Rockwell 500

Analysis

The pilot-in-command seated in the right seat was providing familiarization in the multi-engine airplane to the left seat pilot during a flight to a nearby airport for fuel. Shortly after takeoff, one of the pilots reported an engine problem and advised that they were diverting to a nearby airport. A witness along the route of flight reported hearing the engines accelerating and decelerating and then popping sounds; several witnesses near the accident site reported hearing no engine sounds. The airplane impacted a building and terrain about 10 minutes after takeoff. Very minimal fuel leakage on the ground was noted and only 23 ounces of aviation fuel were collected from the airplane’s five fuel tanks. No evidence of preimpact failure or malfunction was noted for either engine or propeller; the damage to both propellers was consistent with low-to-no power at impact. Since the pilot could not have visually verified the fuel level in the center fuel tank because of the low quantity of fuel prior to the flight, he would have had to rely on fuel consumption calculations since fueling based on flight time and the airplane’s fuel quantity indicating system. Although the fuel quantity indications at engine start and impact could not be determined postaccident from the available evidence, if the fuel quantity reading at the start of the flight was accurate based on the amount of fuel required for engine start, taxi, run-up, takeoff, and then only to fly the accident flight duration of 10 minutes, it would have been reading between 8 and 10 gallons. It is unlikely that the pilot, who was a chief pilot of a cargo operation and tasked with familiarizing company pilots in the airplane, would have knowingly initiated the flight with an insufficient fuel load for the intended flight or with the fuel gauge accurately registering the actual fuel load that was on-board. Examination of the tank unit, or fuel quantity transmitter, revealed that the resistance between pins A and B, which were the ends of the resistor element inside the housing, fell within specification. When monitoring the potentiometer pin C, there was no resistance, indicating an open circuit between the wiper and the resistor element. X-ray imaging revealed that the conductor of electrical wire was fractured between the end of the lugs at the wiper and for pin C. Bypassing the fractured conductor, the resistive readings followed the position of the float arm consistent with normal operation. Visual examination of the wire insulation revealed no evidence of shorting, burning or damage. Examination of the fractured electrical conductor by the NTSB Materials Laboratory revealed that many of the individual wires exhibited intergranular fracture surface features with fatigue striations in various directions on some individual grains. It is likely that the many fatigue fractured conductor strands of the electrical wire inside the accident tank unit or fuel transmitter resulted in the fuel gauge indicating that the tanks contained more fuel than the amount that was actually on board, which resulted in inadequate fuel for the intended flight and a subsequent total loss of engine power due to fuel exhaustion. The inaccurate fuel indication would also be consistent with the pilot’s decision to decline additional fuel before departing on the accident flight. While the estimated fuel remaining since fueling (between 15 and 51 gallons) was substantially more than the actual amount on board at the start of the accident flight (between 8 and 10 gallons), the difference could have been caused by either not allowing the fuel to settle during fueling, and/or the operational use of the airplane. Ultimately, the fuel supply was likely completely exhausted during the flight, which resulted in the subsequent loss of power to both engines. Given the circumstances of the accident, the effects from the right seat pilot’s use of cetirizine and the identified ethanol in the left seat pilot, which was likely from sources other than ingestion, did not contribute to this accident.

Factual Information

HISTORY OF FLIGHTOn August 28, 2020, about 0902 eastern daylight time, an Aero Commander 500-S, N900DT, was destroyed when it impacted a building near Pembroke Park, Florida. The commercial pilot and airline transport pilot were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 familiarization flight. The purpose of the flight was for the right-seat pilot, who was pilot-in-command, to familiarize the left-seat pilot with the airplane. Two individuals associated with the facility that maintained the airplane asked the pilot whether he wanted to fuel the airplane or have it towed to the fuel pump. The pilot responded that he planned to fuel the airplane at the intended destination, Miami-Opa Locka Executive Airport (OPF), Miami, Florida. According to Federal Aviation Administration (FAA) Automatic Dependent Surveillance – Broadcast (ADS-B) and air traffic control information, after takeoff about 0852, the airplane proceeded in a southeast direction to the shore, then flew in a south-southwest direction just offshore. About 0858, when the airplane was about 13 nautical miles northeast of OPF, an occupant of the airplane contacted the OPF air traffic control tower and advised the controller that the airplane was inbound. The airplane continued in a south-southwesterly direction while climbing to 1,100 ft mean sea level (msl). At 0859:49, or 1 minute 49 seconds after the initial contact with the tower controller, an occupant advised the controller of an “engine problem” and that they would be diverting to North Perry Airport (HWO), Hollywood, Florida. The controller approved the frequency change and initially coordinated with Miami Approach and advised the facility that the airplane was descending, with a last reported altitude of 300 ft. At 0859:53, the airplane turned to the southwest and climbed to about 1,250 ft msl. A witness located about 2.8 nautical miles east-southeast of the flightpath reported hearing the engines accelerating and decelerating, which changed to a popping sound. The airplane continued flying out of his earshot. The ADS-B data reflected that, at 0900:47, the airplane turned and flew in a west-northwesterly direction until 0901:58, when it proceeded in a north-northwesterly direction until near the accident site. Witnesses on a golf course north of the accident site reported seeing the airplane flying in a westerly direction with no sound coming from the engines. They noted that the airplane banked left and descended. Another witness, located about 440 ft northeast of the accident site, reported hearing no sound from the airplane before impact. The witness reported that the right wing impacted the building and the airplane rotated to the left. The airplane then fell to the parking lot of the building. There were no ground injuries. PERSONNEL INFORMATIONThe pilot seated in the right seat was the chief pilot for a 14 CFR Part 135 cargo operation. He was tasked by his company to familiarize company pilots in the airplane. The mobile phone of the left seat pilot did not contain any video of the accident date or personal data (text messages, emails, personal photos/videos, app usage) relevant to the investigation. It did contain a series of google searches and visited web pages related to airplane performance taken 5 days before the accident and one video taken 4 days before the accident, which depicted the accident airplane taxiing on an airport ramp. There was nothing anomalous about the accident aircraft’s operation or condition displayed in the video. AIRCRAFT INFORMATIONThe airplane was manufactured in 1969. At the time of manufacture, certification standards specified that the fuel quantity gauge shall be calibrated to read zero during level flight when the quantity of fuel remaining in the tank is equal to the unusable fuel supply. The airplane’s fuel system comprised five interconnected synthetic rubber cells installed in the inboard and center wing sections, having a total usable capacity of 156 gallons. All fuel cells were serviced through a single filler port, located on top of the right wing above the forward fuel cell. The fuel quantity was measured by a single transmitter or tank unit installed in the center wing fuel cell and electrically connected to a fuel quantity indicator located in the instrument panel. An optional Fuel Low Level Warning System was not installed. Section II of the maintenance manual, titled “Ground Handling, Servicing and Airframe Maintenance,” contained special inspection requirements for the fuel system which indicated, “whenever any component which would effect calibration is replaced and every 1,000 hours or annual” to, “check fuel quantity system for correct calibration.” It also indicated that, every 1,000 hours, the transmitter be checked for specified wiper arm tension and internal corrosion, the cover, and connector plug for safety. The airplane’s most recent annual inspection was signed off as being completed on August 14, 2020, “[in accordance with 14 CFR Part] 43 Appendix D, using Aero Commander 500 S [Maintenance Manual] CH 5 [inspection] checklist as a guide….” The recorded airplane total time at the annual inspection was 10,300.9 hours. Appendix D of 14 CFR Part 43 specified to inspect, in part, the, “Instruments--for poor condition, mounting, marking, and (where practicable) improper operation.” The Gulfstream Aerospace Corporation Airframe and Powerplant 100 Hour Inspection Form utilized by the maintenance facility for the last annual inspection specified in part, “Check all instruments” with a mechanic’s initials next to the line. Neither 14 CFR Part 43 Appendix D or the inspection form utilized by the facility specified calibrating the fuel quantity indicating system. A review of nearly 51 years of available maintenance records for work performed to the tank unit or fuel quantity transmitter, fuel quantity gauge, or calibration of the fuel quantity indicating system revealed one entry on December 11, 1981. The entry indicated, in part, that a 1,000-hour inspection of the tank unit or fuel quantity transmitter was performed at an airplane total time of 3,086.0 hours. Although replacement of the fuel quantity indicator was not documented in the maintenance records, its markings indicated that it was manufactured on January 31, 1983. Thus, the airplane had been operated about 7,215 hours and nearly 39 years since the last documented work was performed to the fuel quantity transmitter and a maximum of about 37 1/2 years since the fuel quantity indicator was replaced. The pilot was reportedly advised by maintenance personnel to operate the engines with the mixture controls full rich because both engines had been “top overhauled” in February 2019, and were still being broken in. As of the annual inspection two weeks earlier, the airplane had accrued between 2 and 33 hours since the cylinder work for both engines was performed. According to the engine Operator’s Manual, following cylinder replacement or top overhaul of one or more cylinders until a total of 50 hours has been accumulated, cruise flight should be performed at 65% to 75% power. It did not specify that the engine must be operated with the mixture control full rich, but did state that for maximum service life, cylinder head temperatures should be maintained below 435°F during high performance cruise and below 400°F for economy cruise power settings. According to flight planning data from the Aircraft Flight Manual (AFM), the fuel required for engine start, taxi, run-up and takeoff was 25 pounds, or about 4.2 gallons. The fuel flow in terms of pounds-per-hour (pph) of each engine at 65% and 75% power varied with engine rpm and whether the fuel-to-air ratio was leaned to best power (leaned to peak exhaust gas temperature (EGT) then enrichened 150°F), or best economy (leaned to peak EGT). At 65% power, the fuel flow ranged from 74 to 92 pph. The fuel flow at 75% power ranged from 86 to 103 pph. The AFM did not have any fuel consumption data for full rich mixture settings. The airplane was most recently fueled with 51.4 gallons of 100 low lead aviation fuel on August 19, 2020, at OPF. According to an individual who performed the fueling, the fuel request was a top off. He indicated that he completely topped off, “1 tank on the right wing while the crew was present. Also, [the accident flight right seat pilot by name] checked the fuel tank after I was done and told me that it was ok. That is when I disconnected & finished up.” Based on ADS-B data since fueling excluding the accident flight, the airplane had been operated about 3 hours 42 minutes on three separate flights, the last being August 24, 2020. In some instances, the ADS-B data did not include taxi times; therefore, the actual duration of the flights since fueling including taxi time could not be determined. The pilot of the accident flight was on board the airplane during all three flights. Fuel consumption calculations were performed using the lowest and highest fuel flow range specified by the airframe manufacturer at 65% and 75% power, multiplied by 3.75 hours, plus fuel used for three takeoffs (12.6 gallons). The calculated total consumption since fueling, excluding the accident flight, was between about 105 and 141 gallons. Postaccident calculations to determine the approximate amount of fuel on board to start the flight and then fly 10 minutes (accident flight duration) were performed. The calculations included the amount of fuel used for engine start through takeoff (4.2 gallons), the lowest and highest fuel flow range specified by the airframe manufacturer at 65% and 75% power, multiplied by the accident flight duration (.16 hour). Between 8 and 10 gallons were required. That amount did not include the unusable fuel amount. A review of reports from the FAA Service Difficulty Program for the 500 series aircraft fuel system from January 1, 2012 through June 28, 2022, revealed two reports, both in 2012. One report was associated with an off-airport forced landing of a model 500B airplane due to “fuel starvation” though the fuel gauge indicated 60 gallons of fuel. A mechanic found a broken wire in the transmitter variable contact of the tank unit or fuel transmitter that was same part number as the one installed in the accident airplane. That incident was not investigated by NTSB. The other report, also associated with a 500B airplane, indicated that, as a result of the off-airport forced landing of the other airplane due to “fuel starvation,” they inspected the tank unit or fuel transmitter and found a “…brittle wire on the transmitter variable contact making [intermittent] connection.” The submitter suggested an internal inspection of the tank unit or fuel transmitter at 100-hour and/or annual inspections to verify that all contacts, wires, and internal parts are secure, in good condition and working properly. AIRPORT INFORMATIONThe airplane was manufactured in 1969. At the time of manufacture, certification standards specified that the fuel quantity gauge shall be calibrated to read zero during level flight when the quantity of fuel remaining in the tank is equal to the unusable fuel supply. The airplane’s fuel system comprised five interconnected synthetic rubber cells installed in the inboard and center wing sections, having a total usable capacity of 156 gallons. All fuel cells were serviced through a single filler port, located on top of the right wing above the forward fuel cell. The fuel quantity was measured by a single transmitter or tank unit installed in the center wing fuel cell and electrically connected to a fuel quantity indicator located in the instrument panel. An optional Fuel Low Level Warning System was not installed. Section II of the maintenance manual, titled “Ground Handling, Servicing and Airframe Maintenance,” contained special inspection requirements for the fuel system which indicated, “whenever any component which would effect calibration is replaced and every 1,000 hours or annual” to, “check fuel quantity system for correct calibration.” It also indicated that, every 1,000 hours, the transmitter be checked for specified wiper arm tension and internal corrosion, the cover, and connector plug for safety. The airplane’s most recent annual inspection was signed off as being completed on August 14, 2020, “[in accordance with 14 CFR Part] 43 Appendix D, using Aero Commander 500 S [Maintenance Manual] CH 5 [inspection] checklist as a guide….” The recorded airplane total time at the annual inspection was 10,300.9 hours. Appendix D of 14 CFR Part 43 specified to inspect, in part, the, “Instruments--for poor condition, mounting, marking, and (where practicable) improper operation.” The Gulfstream Aerospace Corporation Airframe and Powerplant 100 Hour Inspection Form utilized by the maintenance facility for the last annual inspection specified in part, “Check all instruments” with a mechanic’s initials next to the line. Neither 14 CFR Part 43 Appendix D or the inspection form utilized by the facility specified calibrating the fuel quantity indicating system. A review of nearly 51 years of available maintenance records for work performed to the tank unit or fuel quantity transmitter, fuel quantity gauge, or calibration of the fuel quantity indicating system revealed one entry on December 11, 1981. The entry indicated, in part, that a 1,000-hour inspection of the tank unit or fuel quantity transmitter was performed at an airplane total time of 3,086.0 hours. Although replacement of the fuel quantity indicator was not documented in the maintenance records, its markings indicated that it was manufactured on January 31, 1983. Thus, the airplane had been operated about 7,215 hours and nearly 39 years since the last documented work was performed to the fuel quantity transmitter and a maximum of about 37 1/2 years since the fuel quantity indicator was replaced. The pilot was reportedly advised by maintenance personnel to operate the engines with the mixture controls full rich because both engines had been “top overhauled” in February 2019, and were still being broken in. As of the annual inspection two weeks earlier, the airplane had accrued between 2 and 33 hours since the cylinder work for both engines was performed. According to the engine Operator’s Manual, following cylinder replacement or top overhaul of one or more cylinders until a total of 50 hours has been accumulated, cruise flight should be performed at 65% to 75% power. It did not specify that the engine must be operated with the mixture control full rich, but did state that for maximum service life, cylinder head temperatures should be maintained below 435°F during high performance cruise and below 400°F for economy cruise power settings. According to flight planning data from the Aircraft Flight Manual (AFM), the fuel required for engine start, taxi, run-up and takeoff was 25 pounds, or about 4.2 gallons. The fuel flow in terms of pounds-per-hour (pph) of each engine at 65% and 75% power varied with engine rpm and whether the fuel-to-air ratio was leaned to best power (leaned to peak exhaust gas temperature (EGT) then enrichened 150°F), or best economy (leaned to peak EGT). At 65% power, the fuel flow ranged from 74 to 92 pph. The fuel flow at 75% power ranged from 86 to 103 pph. The AFM did not have any fuel consumption data for full rich mixture settings. The airplane was most recently fueled with 51.4 gallons of 100 low lead aviation fuel on August 19, 2020, at OPF. According to an individual who performed the fueling, the fuel request was a top off. He indicated that he completely topped off, “1 tank on the right wing while the crew was present. Also, [the accident flight right seat pilot by name] checked the fuel tank after I was done and told me that it was ok. That is when I disconnected & finished up.” Based on ADS-B data since fueling excluding the accident flight, the airplane had been operated about 3 hours 42 minutes on three separate flights, the last being August 24, 2020. In some instances, the ADS-B data did not include taxi times; therefore, the ac

Probable Cause and Findings

A total loss of engine power due to fuel exhaustion. Contributing to the fuel exhaustion was the fatigue fracture of an electrical wire in the tank unit or fuel transmitter, which likely resulted in an inaccurate fuel quantity indication.

 

Source: NTSB Aviation Accident Database

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