Aviation Accident Summaries

Aviation Accident Summary WPR22FA094

Glendale, AZ, USA

Aircraft #1

N633AX

DASSAULT AVIATION MIRAGE F1 CR

Analysis

A turbo-jet airplane was being operated as a public-use aircraft in support of the United States Air Force’s simulated combat flight training at the time of the accident. The airplane took off and proceeded to the Military Operating Area (MOA) and, near the completion of the flight the pilot reported a discrepancy between the two fuel quantity indications in the cockpit. Shortly thereafter, the pilot headed back to the airport once the airplane reached its briefed minimum fuel status. While en route to the airport, the pilot reported a loss of fuel pressure and shortly afterward the engine flamed out. The pilot attempted to restart the engine but was unsuccessful. When the pilot determined that he could not make the runway at his destination, he turned toward an uninhabited area and successfully ejected from the airplane. Subsequently, the airplane impacted terrain. Postaccident interviews revealed that the airplane was not fueled with the correct amount of fuel for the flight by maintenance personnel before the flight. Although the refueling forms accurately reflected the shorted amount of fuel, the error was not detected by maintenance personnel or the pilot before the airplane took off. During the flight, the pilot failed to notice that his fuel load was incorrect. The pilot relied on a fuel remaining totalizer that had been manually set to the expected full fuel load, not to the actual fuel load, and did not appropriately reference the individual fuel quantity tapes. Postaccident examination of the airplane wreckage revealed that the airplane’s fuel tanks had loose sealant globules inside the main feeder fuel tanks and an additional piece of Foreign Object Debris (FOD) present. Additionally, the operator discovered that several of their F-1 airplanes were found with varies type of FOD in the fuel tanks, including loose pieces of fuel tank sealant, which led to fuel anomalies including issues that caused false full tank fuel indications during refueling. Once the FOD was removed, the airplanes’ fuel system anomalies that were experienced were virtually eliminated. It is possible that the FOD caused anomalies during refueling of the accident airplane and presented a false full tank indication, which contributed to the airplane not being serviced to the correct fuel load.

Factual Information

HISTORY OF FLIGHTOn February 10, 2022, about 1105 mountain standard time, an experimental Dassault Aviation Mirage F-1 CR Turbo-jet, N633AX, was destroyed when it was involved in an accident near Luke Air Force Base, (LUF), Glendale, Arizona. The pilot sustained minor injuries. The airplane was operated as a public-use aircraft in support of the United States Air Force’s simulated combat flight training. According to the accident pilot, he flew in the number two position in a flight of two aggressor jets. The formation took off and proceeded to the MOA, where the two airplanes split up into separate areas. Near the completion of the area work, the pilot reported a discrepancy between the two fuel quantity indications in the cockpit. Shortly thereafter, he recovered before the lead airplane since his airplane reached its briefed minimum fuel status first. While exiting the MOA, and en route on the recovery, the pilot reported a loss of fuel pressure and shortly afterward the engine flamed out. The pilot attempted to restart the engine but was unsuccessful. When the pilot determined that he could not make it back to the runway at LUF, he executed a left turn to an uninhabited area and successfully ejected from the airplane. Subsequently, the airplane struck desert terrain about 16 miles northwest of LUF. Postaccident interviews revealed that the airplane was not fueled with the correct amount of fuel for the flight by maintenance personnel before the flight. Although the refueling forms accurately reflected the shorted amount of fuel, the error was not detected by maintenance personnel or the pilot before the airplane took off. During the flight, the pilot failed to notice that his fuel load was incorrect. A high throttle setting (with frequent afterburner use) basic fighter maneuver flight engagement for the pilot, made him rely on the fuel remaining totalizer, without appropriately referencing the individual fuel quantity tapes. The fuel remaining totalizer that the pilot relied on had been manually set to the expected full fuel load, not to the actual fuel load. Subsequently, the low fuel light illuminated in the MOA and during the return to LUF, the fuel quantity tapes indicated zero, while the fuel totalizer read about 1,300 liters. Shortly afterwards, the engine flamed out consistent with fuel exhaustion. PERSONNEL INFORMATIONThe pilot held an airline pilot certificate with a flight instructor airplane single-engine and multi-engine land and airplane instrument ratings. He also held an experimental aircraft authorization for the DA-F1. The pilot was issued a Federal Aviation Administration (FAA) first-class medical certificate on July 20, 2021, without limitations. The pilot reported about 4,859 total hours of flight experience and about 240 hours in the F-1 aircraft. He was a former military fighter pilot in the F-16 and F-18 aircraft and an airline pilot. According to the pilot of the lead aircraft and maintenance personnel that launched the airplane, the accident pilot appeared to be in a normal good mood the day of the accident. The accident pilot stated that he had normal sleep the 3 days before the accident and had no personal issues to report. AIRCRAFT INFORMATIONThe F-1 Mirage was a French fighter and attack aircraft that was imported into the United States and registered under the experimental category. It is a single-engine, swept-wing, supersonic airplane capable of Mach 2.1. The airplane had a maximum takeoff weight of over 35,000 lbs. The airplane’s fuel system is comprised of a left and right fuel system. Normally, the left and right fuel systems are isolated from each other but can be connected to each other through a crossfeed valve. Refueling is normally carried out by pressurized single point refueling. The total quantity of usable fuel was about 4,100 liters. This total does not include the use of the optional external centerline fuel tank, which increased the fuel capacity by about 1,180 liters. The airplane was equipped with 9 internal fuel tanks (including the 2 feeder tanks), 2 internal wing tanks, and 2 negative-g flight accumulators. Engine air pressure moves the fuel to the feeder tanks and from there it flows directly to the engine by 2 low pressure pumps. The F-1 refueling checklist indicated for a clean airplane the following fuel capacity (in liters): The airplane fuel gauges consisted of 2 vertical tapes that indicated the fuel quantity on the left and right side. The wing tanks and optional external tanks are not gauged. The fuel tapes only indicate about a maximum of about 2,000 liters of fuel on each side and, therefore, the tape indications would only start to decrease when the airplane had less than about 4,000 liters of total fuel. The fuel transfer sequence is designed so that the optional external fuel tanks are consumed first, then the wing tanks, and then the gauged internal fuel tanks. Usually, once the airplane’s external centerline and wing tanks are empty, the tape indications should reflect what the fuel remaining indicator (a 4-figure counter measured in liters) indicated. With more than 2,000 liters of fuel in each tank, the tapes would indicate near the full indication. In addition, the fuel remaining indicator (totalizer) would be manually preset to the total quantity of fuel onboard before flight and would decrease according to how much fuel the airplane used. The accident airplane was refueled the day before the accident. During the start of the refueling the nozzle pressure was kept at 20 psi to ensure that the airplane took fuel and did not overpressure and vent fuel. About three minutes into the refueling, the fuel truck driver observed a significant amount of fuel venting from the airplane and was instructed to stop refueling by the operator’s maintenance personnel. The driver said it was the most venting he had seen during his one year of refueling the F-1. After having stopped for a couple of minutes, the operator’s maintenance personnel checked the airplane and placed the collection container back to collect fuel that vented overboard and the refueling was resumed. Subsequently, about 7 minutes later, a total of about 456 gallons (about 1,726 liters) was added to the airplane and then the refueling driver observed a spike in back pressure that was a characteristic of the jet being fully loaded with fuel and stopped refueling. In addition, the operator’s refueling personnel monitoring the refueling thought the refueling was complete as well. However, the fuel added was not to the full fuel load amount that was normally serviced. Given, that the airplane’s shutdown fuel from the previous flight was 2,320 liters and the fuel serviced was 1,726 liters, the airplane’s fuel load for the accident flight after refueling was about 4,046 liters, which was less the normal full fuel load of about 5,280 liters with the external center fuel tank that was installed. Additionally, an engine run of about 10 minutes for maintenance took place on the airplane before takeoff and no fuel was added afterward. Therefore, the fuel load for takeoff was slightly lower than 4,046 liters. Maintenance personnel and the pilot then reviewed the aircraft forms, which indicated the amount of fuel serviced, but did not detect the shorted amount of fuel added. Additionally, during the ground refueling process, the refueling lights flash on and then go out when the corresponding tanks are full. The last step of the checklist was to manually set the fuel remaining quantity indicator (totalizer) to display the amount of fuel in the airplane. The fuel remaining quantity indicator was as if the airplane was fully fueled with 5,280 liters of fuel. On the airplane’s warning and caution panel, the FUEL PRES red light would illuminate when the engine inlet fuel pressure was < 700 mb (10.15 psi). The LOW FUEL red light would illuminate when either feeder fuel tank was < 250 liters. A red warning light illumination called for immediate action by the pilot. The emergency procedure for a FUEL PRES red warning light, which indicated that the dry engine fuel pressure was less than 700 mb while airborne, was to shut down use of AB and reduce rpm, check LP pumps on, check left and right LP caution lights out, and land as soon as possible while monitoring the fuel totalizer and both fuel gauges for indications of a fuel leak. The emergency procedure for LOW FUEL warning light was to select the emergency transfer switch forward or aft as required, which connected the left and right forward or aft tanks (depending on selection) and allowed transfer of both tanks to the same feed tank. If the quantity of both feed tanks was below 250 liters and transfer sequence was normal, with or without tank 3 illuminated, the procedures were: - RPM reduce. - Descend to below 20,000 ft, heading to nearest field. - RPM – set 8,000 for 30 seconds (maximum) and check the feed tank quantity. - If the feed tank transfer does not increase – use emergency transfer. - If the feed tank quantity increases – if necessary, continue flight at no higher than current altitude (< 20,000 ft). - Land as soon as possible. The operator performed a daily inspection on the accident airplane before its flight. Additionally, the airplane’s last 100-hour inspection was accomplished on November 2, 2021, at an airframe total time of 6,333.3 hours. AIRPORT INFORMATIONThe F-1 Mirage was a French fighter and attack aircraft that was imported into the United States and registered under the experimental category. It is a single-engine, swept-wing, supersonic airplane capable of Mach 2.1. The airplane had a maximum takeoff weight of over 35,000 lbs. The airplane’s fuel system is comprised of a left and right fuel system. Normally, the left and right fuel systems are isolated from each other but can be connected to each other through a crossfeed valve. Refueling is normally carried out by pressurized single point refueling. The total quantity of usable fuel was about 4,100 liters. This total does not include the use of the optional external centerline fuel tank, which increased the fuel capacity by about 1,180 liters. The airplane was equipped with 9 internal fuel tanks (including the 2 feeder tanks), 2 internal wing tanks, and 2 negative-g flight accumulators. Engine air pressure moves the fuel to the feeder tanks and from there it flows directly to the engine by 2 low pressure pumps. The F-1 refueling checklist indicated for a clean airplane the following fuel capacity (in liters): The airplane fuel gauges consisted of 2 vertical tapes that indicated the fuel quantity on the left and right side. The wing tanks and optional external tanks are not gauged. The fuel tapes only indicate about a maximum of about 2,000 liters of fuel on each side and, therefore, the tape indications would only start to decrease when the airplane had less than about 4,000 liters of total fuel. The fuel transfer sequence is designed so that the optional external fuel tanks are consumed first, then the wing tanks, and then the gauged internal fuel tanks. Usually, once the airplane’s external centerline and wing tanks are empty, the tape indications should reflect what the fuel remaining indicator (a 4-figure counter measured in liters) indicated. With more than 2,000 liters of fuel in each tank, the tapes would indicate near the full indication. In addition, the fuel remaining indicator (totalizer) would be manually preset to the total quantity of fuel onboard before flight and would decrease according to how much fuel the airplane used. The accident airplane was refueled the day before the accident. During the start of the refueling the nozzle pressure was kept at 20 psi to ensure that the airplane took fuel and did not overpressure and vent fuel. About three minutes into the refueling, the fuel truck driver observed a significant amount of fuel venting from the airplane and was instructed to stop refueling by the operator’s maintenance personnel. The driver said it was the most venting he had seen during his one year of refueling the F-1. After having stopped for a couple of minutes, the operator’s maintenance personnel checked the airplane and placed the collection container back to collect fuel that vented overboard and the refueling was resumed. Subsequently, about 7 minutes later, a total of about 456 gallons (about 1,726 liters) was added to the airplane and then the refueling driver observed a spike in back pressure that was a characteristic of the jet being fully loaded with fuel and stopped refueling. In addition, the operator’s refueling personnel monitoring the refueling thought the refueling was complete as well. However, the fuel added was not to the full fuel load amount that was normally serviced. Given, that the airplane’s shutdown fuel from the previous flight was 2,320 liters and the fuel serviced was 1,726 liters, the airplane’s fuel load for the accident flight after refueling was about 4,046 liters, which was less the normal full fuel load of about 5,280 liters with the external center fuel tank that was installed. Additionally, an engine run of about 10 minutes for maintenance took place on the airplane before takeoff and no fuel was added afterward. Therefore, the fuel load for takeoff was slightly lower than 4,046 liters. Maintenance personnel and the pilot then reviewed the aircraft forms, which indicated the amount of fuel serviced, but did not detect the shorted amount of fuel added. Additionally, during the ground refueling process, the refueling lights flash on and then go out when the corresponding tanks are full. The last step of the checklist was to manually set the fuel remaining quantity indicator (totalizer) to display the amount of fuel in the airplane. The fuel remaining quantity indicator was as if the airplane was fully fueled with 5,280 liters of fuel. On the airplane’s warning and caution panel, the FUEL PRES red light would illuminate when the engine inlet fuel pressure was < 700 mb (10.15 psi). The LOW FUEL red light would illuminate when either feeder fuel tank was < 250 liters. A red warning light illumination called for immediate action by the pilot. The emergency procedure for a FUEL PRES red warning light, which indicated that the dry engine fuel pressure was less than 700 mb while airborne, was to shut down use of AB and reduce rpm, check LP pumps on, check left and right LP caution lights out, and land as soon as possible while monitoring the fuel totalizer and both fuel gauges for indications of a fuel leak. The emergency procedure for LOW FUEL warning light was to select the emergency transfer switch forward or aft as required, which connected the left and right forward or aft tanks (depending on selection) and allowed transfer of both tanks to the same feed tank. If the quantity of both feed tanks was below 250 liters and transfer sequence was normal, with or without tank 3 illuminated, the procedures were: - RPM reduce. - Descend to below 20,000 ft, heading to nearest field. - RPM – set 8,000 for 30 seconds (maximum) and check the feed tank quantity. - If the feed tank transfer does not increase – use emergency transfer. - If the feed tank quantity increases – if necessary, continue flight at no higher than current altitude (< 20,000 ft). - Land as soon as possible. The operator performed a daily inspection on the accident airplane before its flight. Additionally, the airplane’s last 100-hour inspection was accomplished on November 2, 2021, at an airframe total time of 6,333.3 hours. WRECKAGE AND IMPACT INFORMATIONExamination of the accident site revealed that the jet airplane impacted flat desert terrain in an unoccupied area between residential areas. All major components of the airplane were found at the main wreckage site. The wreckage site was at an elevation of about 1,622 ft msl. There was no postimpact fire. There was a large ground disturbance that led to the area where most of the major sections of the airplane were located. The initial point of impact was orientated on a heading of about 060° magnetic. The aft portion of the fuselage (the largest portion of fuselage that remained relatively intact) came to rest inverted. Small fragments of aircraft debris

Probable Cause and Findings

A loss of engine power due to fuel exhaustion as result of the failure of maintenance personnel to ensure the airplane was serviced with the correct amount of fuel, the failure of maintenance personnel and the pilot to adequately check the airplane’s paperwork to ensure the correct amount of fuel was present for the flight, and the failure of the pilot to adequately monitor the airplane’s fuel status during the flight.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports