Aviation Accident Summaries

Aviation Accident Summary ERA22LA169

Smithfield, NC, USA

Aircraft #1

N471BL

DIAMOND AIRCRAFT IND INC DA 40 NG

Analysis

According to the flight instructor, shortly after takeoff, she heard a “weird” noise coming from the engine and noted a drop in engine rpm. The flight instructor directed the pilot receiving instruction to turn back toward the airport; however, the engine lost all power, and the airplane impacted trees about 1 mile from the departure end of the runway. The airplane sustained substantial damage to the wings, fuselage, and empennage. A postaccident examination of the engine revealed that the engine valvetrain was not timed correctly and that the misalignment resulted in a piston striking a valve. The valve head had separated and fallen into the cylinder, resulting in the total loss of engine power. Examination of the maintenance logbooks revealed that the cylinder head and exhaust camshaft had been replaced the day before the accident flight. Thus, it is likely that the engine’s timing was not set correctly after this maintenance.

Factual Information

On March 25, 2022, about 1613 eastern daylight time, a Diamond DA-40NG, N471BL, was substantially damaged when it was involved in an accident near Johnston Regional Airport (JNX), Smithfield, North Carolina. The flight instructor and pilot receiving instruction were seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight. According to the flight instructor and pilot receiving instruction, they conducted a preflight inspection of the airplane, with no anomalies noted, before departing from runway 21 at JNX. Review of radar data revealed that the airplane climbed to an altitude of about 650 ft while turning left. The flight instructor stated that she “heard a weird noise come from the engine” and saw the rpm gauge drop. Shortly afterward, the flight instructor directed the pilot receiving instruction to turn back to the airport, and the engine lost total power while in the turn. The flight instructor attempted to restart the engine while the airplane descended but was unsuccessful. The airplane subsequently impacted trees about 1 mile from the departure end of the runway, resulting in substantial damage to the fuselage. In addition, both wings and the empennage were fractured from the impact. A postaccident examination of the engine revealed that engine valvetrain was not timed correctly and that the resulting misalignment resulted in the piston striking the valve. The valve head had subsequently separated and fallen into the cylinder. Examination of the maintenance logbooks revealed that the cylinder head and exhaust camshaft had been replaced the day before the accident flight.

Probable Cause and Findings

Maintenance personnel’s failure to set the correct engine timing after the replacement of a cylinder head and exhaust camshaft before the accident flight, which resulted in a total loss of engine power.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports