Aviation Accident Summaries

Aviation Accident Summary WPR22LA352

Lander, WY, USA

Aircraft #1

N5148G

JACQUNEAUX GLEN R CGS HAWK

Analysis

The pilot reported that, about 40 minutes after departure at an altitude of about 9,500 ft mean sea level (msl), he decided to land off-airport due to severe up and down shaking of the experimental airplane’s empennage. The pilot reduced the throttle setting and initiated a glide. The pilot observed that the airplane remained stable during the glide, with no extreme vibration, and that he was able to manage the descent smoothly. Shortly after touchdown, the airplane bounced and landed hard on a field. Subsequently, the airplane nosed over and sustained substantial damage to the tail assembly.  The wreckage was recovered from a field onto a flatbed truck by a local resident. The National Transportation Safety Board (NTSB) investigator-in-charge (IIC) interviewed the pilot after the accident and requested that he preserve the wreckage; however, the pilot had given the wreckage to the local resident who helped with the recovery. The pilot added that he was returning to his home country in two weeks when his visa expired. A Federal Aviation Administration (FAA) inspector took pictures of the airplane on top of the flatbed truck but was unable to conduct an examination of the airframe or engine. The pilot further reported during a follow-up interview that he believed the engine and frame installed were too heavy for the airframe, which resulted in the extreme airframe vibration. He added that the engine was from a pre-owned car and had been installed about 7 years before the accident. The pilot indicated that the violent shaking during the accident sequence was the first occurrence in the airplane's last 204 hours of flight, which spanned the last 90 days. The local resident reported that during the recovery process, the pilot admitted to using zip ties to keep sections of the airplane intact. The pilot was not responsive after several attempts to coordinate a follow-up examination. Moreover, despite several attempts, the local resident did not respond to the investigator’s request to examine the wreckage. Since the wreckage was not made available for examination, the reason for the reported airframe vibration could not be determined.

Factual Information

On September 15, 2022, about 1442 mountain daylight time, an experimental CGS Hawk, N5148G, was substantially damaged when it was involved in an accident near Lander, Wyoming. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot reported that he was on a cross-country flight that originated on August 28, 2022, with the final destination being Isabell Field Airport (4A9), Fort Payne, Alabama. On the day of the accident, he departed Hunt Field Airport (KLND), Lander, Wyoming, and was enroute to the Kimball Municipal Airport (IBM), Kimball, Nebraska. About 40 minutes after departure and about 9,500 ft mean sea level (msl), the empennage section started to violently shake up and down. The pilot decided to execute an off-airport landing; he decreased the throttle setting and started a glide. The pilot stated that the airplane was stable during the glide without any excessive vibration and that he was able to smoothly control the airplane. Shortly after touchdown, the airplane bounced and landed hard on sloped and uneven terrain. Subsequently, the airplane nosed over and sustained substantial damage to the tail assembly. Law enforcement officials reported that the pilot received assistance from a local resident who discovered the airplane and the pilot in a field. The local resident helped the pilot move the airplane from the field onto a flatbed truck. The local resident reported that during the recovery process, the pilot admitted to using zip ties to keep sections of the airplane intact. In addition, the pilot expressed his disinterest in keeping the airplane and he sent a digital copy of the airplane’s title to him via text message. An FAA inspector was able to take pictures of the airplane disassembled on a flatbed truck, but he was not able to conduct an examination of the engine or airframe. The pilot stated that he purchased the airplane about a month before the accident. He added that the installed engine was a pre-owned car engine, which had accumulated about 59,000 miles before being installed on the airplane about 7 years before the accident. He believed that the installed engine and frame were too heavy for the airframe. According to the pilot, this was the first time in the last 90 days, which amounted to about 204 flight hours, that the empennage section had a violent shake during flight. The pilot reported that his visa would expire about two weeks after the accident, and that he would be returning to his home country. Despite repeated attempts to reach the pilot after the initial interview, the NTSB IIC did not receive a response. In addition, despite numerous phone calls, the local resident did not respond to a request to examine the wreckage.

Probable Cause and Findings

A reported severe airframe vibration and subsequent forced landing for reasons that could not be determined because the wreckage was not made available for examination.

 

Source: NTSB Aviation Accident Database

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